N2838T

Substantial
None

Piper PA-28-140S/N: 28-7225247

Accident Details

Date
Wednesday, October 23, 2002
NTSB Number
MIA03LA006
Location
Las Palmas, PR
Event ID
20021024X05380
Coordinates
18.220283, -66.589279
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

The pilot's failure to switch fuel tanks resulting in a partial loss of engine power due to fuel starvation during a go-around. Additionally, the pilot's failure to monitor airspeed and proper touchdown point during the emergency landing resulted in another go-around attempt with partial power and inadequate airspeed that caused a collision with a field off the end of the runway.

Aircraft Information

Registration
N2838T
Make
PIPER
Serial Number
28-7225247
Engine Type
Reciprocating
Year Built
1972
Model / ICAO
PA-28-140P28A
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
EAST WING AVIATION INC
Address
HC-02 BOX 11522
Status
Deregistered
City
HUMACAO
State / Zip Code
PR 00791
Country
United States

Analysis

On October 23, 2002, about 1600 Atlantic standard time, a Piper PA-28-140, N2838T, registered to East Wing Aviation, Inc., operating as a Title 14 CFR Part 91 personal flight, crashed in the vicinity of Las Palmas, Puerto Rico. Visual meteorological conditions prevailed and no flight plan was filed. The airplane was substantially damaged, and the private rated pilot and two passengers were not injured. The flight originated from Humacao, Puerto Rico, about 30 minutes before the accident.

According to the pilot, he realized that he was too high for a safe landing to Patillas Airport's runway 10, and elected to conduct a go-around. During the go-around, at 400 to 500 feet agl, the engine lost partial power, and his best option was to perform a 180- degree course reversal and attempt an emergency landing on runway 28. His touchdown occurred about runway mid-length with excessive approach speed. He attempted a partial power go-around, cleared the airport perimeter fence, and collided with the terrain on the other side of the fence due to insufficient airspeed. The surface of the terrain was rough dirt and grass, and the landing gear collapsed.

According to an FAA inspector, following examination of the wreckage and interviewing the pilot, during the pilot's go-around from runway 10, a partial engine power loss necessitated his attempting to make an emergency approach and landing to runway 28. That approach resulted in a long, fast touchdown due to a tailwind, and the pilot again attempted a go-around. During the second go-around, using partial engine power, the pilot had to effect an abrupt pull-up to miss a fence at the departure end of runway 28. The fence was cleared, but the aircraft crashed in a field on the other side of the fence, collapsing the three landing gear and striking the propeller. The right fuel tank was found empty, and the pilot admitted he did not switch tanks from right to left tank since his departure from Humacao. The left fuel tank contained about 18 gallons of 100 octane LL fuel, which was the quantity observed before departure. The underside of the wings and fuselage revealed no evidence of fuel leakage.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA03LA006