N9288M

Substantial
None

Mooney M20ES/N: 1221

Accident Details

Date
Monday, November 4, 2002
NTSB Number
DEN03LA013
Location
Broomfield, CO
Event ID
20021118X05476
Coordinates
39.908611, -107.117225
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

the pilot's failure to maintain directional control after landing due to a sheared steering horn attach bolt that should have been replaced by maintenance personnel in compliance with an outstanding service bulletin. Contributing factors included the pilot's improper aircraft handling (relaxing elevator back pressure at high speed during rollout) and the ditch.

Aircraft Information

Registration
Make
MOONEY
Serial Number
1221
Engine Type
Reciprocating
Year Built
1966
Model / ICAO
M20EM20P
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
M20E

Registered Owner (Current)

Name
HOGUE MARC A
Address
1753 E BROADWAY RD STE 101-513
City
TEMPE
State / Zip Code
AZ 85282-1590
Country
United States

Analysis

On November 3, 2002, at 1734 mountain standard time, a Mooney M20E, N9288M, registered to and operated by the pilot, was substantially damaged when it exited the runway and collided with a drainage ditch during landing at Jeffco Airport, Broomfield, Colorado. The private pilot and two passengers were uninjured. Visual meteorological conditions prevailed, and no flight plan had been filed for the personal flight being conducted under Title 14 CFR Part 91. The local flight originated at Broomfield approximately 1600.

The following is based on telephone conversations with the pilot and his accident report. He said he made a full flap landing on runway 29R. Instead of keeping the nose wheel off the runway, he relaxed elevator back pressure. When the nose wheel contacted the runway, the airplane swerved to the left. The pilot attempted to straighten the airplane using right rudder and brakes, but to no avail and he lost directional control. The airplane went off the runway and traveled across snow-covered grass. The right main and nose landing gears collapsed, and the airplane slid to a halt on the upslope side of a drainage ditch parallel to the runway.

According to a Beegles Aircraft Services employee who examined the airplane, he found "the steering horn attach bolt sheared at the nut end and the bolt head was slightly backed away from the nose gear truss where it attaches." The employee noted that the sheared AN3-20A bolt was supposed to have "been replaced by a NAS623-3-29 screw as per Mooney Service Bulletin M20-169, dated July 18, 1968. This had not been accomplished. No discrepancies were noted...with the brakes." It could not be determined if the bolt had sheared prior to or upon touchdown or during the impact sequence.

In a subsequent telephone conversation, the pilot said that in retrospect he thought he could have minimized the damage to his airplane. Instead of relaxing elevator back pressure after the airplane touched down, he should have held the nose wheel off the runway as long as possible. In so doing, speed would have dissipated and he could have kept the airplane on the runway by using differential braking.

According to Rocky Mountain Straight Flight, the facility assigned by the pilot to repair the airplane, damage consisted of collapsed right main and nose landing gears, buckled wing and nose gear attach points, firewall, several wing ribs, and crushed wing tips and tail cone.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# DEN03LA013