N1072N

Substantial
None

Mooney M20JS/N: 24-1145

Accident Details

Date
Monday, November 11, 2002
NTSB Number
LAX03LA029
Location
FULLERTON, CA
Event ID
20021122X05511
Coordinates
33.866664, -117.966667
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The pilot's inadequate preflight inspection resulting in a loss of engine power due to water contamination of the fuel system.

Aircraft Information

Registration
Make
MOONEY
Serial Number
24-1145
Engine Type
Reciprocating
Year Built
1981
Model / ICAO
M20JM20P
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
M20J

Registered Owner (Current)

Name
STEPHENS DONALD G
Address
18922 DELAWARE ST UNIT 315
City
HUNTINGTON BEACH
State / Zip Code
CA 92648-6076
Country
United States

Analysis

On November 11, 2002, at 1130 Pacific standard time, a Mooney M20J, N1072N, experienced a loss of engine power during takeoff from runway 24, and executed a forced landing in an open field near the Fullerton Municipal Airport (FUL), Fullerton, California. The airplane was operated by the pilot/owner under the provisions of 14 CFR Part 91, and sustained substantial damage. The private pilot and one passenger were not injured. Visual meteorological conditions prevailed for the personal cross-country flight, and no flight plan had been filed. The flight was scheduled to terminate at the Brown Field Municipal Airport (SDM), San Diego, California.

According to the pilot's written statement, there were no discrepancies noted with the takeoff roll. During the climb out, he retracted the landing gear. As the landing gear came up, the engine "started to die." The pilot stated that there was not enough runway left to land on, so he aimed the airplane for a level field west of the departure end of the runway. The pilot indicated that as the airplane crossed over a fence and road he had to bank slightly to the right to keep from hitting the "understructure" for the runway lights on the airport. The right wing hit the ground first, and the airplane came to rest on its belly.

In a telephone interview with the National Transportation Safety Board investigator-in-charge, the pilot stated that he had completed a preflight check prior to takeoff, which included checking the fuel. The pilot noted no discrepancies with the fuel or fuel system. According to the pilot, the last time the airplane was flown and refueled was approximately 1 week prior to the accident.

A Federal Aviation Administration (FAA) inspector examined the airplane on scene. He found that the right fuel tank was full, and the left fuel tank held about 26 gallons. The fuel selector valve was observed in the off position. The inspector stated that he drained about 32 ounces of water from the right fuel tank sump. The fuel drained from the left fuel tank sump appeared blue in color with no trace of water contamination. He further indicated that water was found in the fuel distribution valve. The FAA inspector interviewed the pilot. The pilot stated he had selected the right fuel tank, the fullest tank, for takeoff.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX03LA029