N5891E

Substantial
None

Cessna 172NS/N: 17271953

Accident Details

Date
Friday, December 6, 2002
NTSB Number
ATL03LA024
Location
Cartersville, GA
Event ID
20021223X05629
Coordinates
34.125000, -84.848609
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The student pilot's failure to maintain directional control, during the landing roll resulted in the on ground collision with a ravine.

Aircraft Information

Registration
N5891E
Make
CESSNA
Serial Number
17271953
Engine Type
Reciprocating
Year Built
1978
Model / ICAO
172NC172
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
LAN AVIATION INC
Address
6015 ATLANTIC BLVD STE D
Status
Deregistered
City
NORCROSS
State / Zip Code
GA 30071-1343
Country
United States

Analysis

On December 6, 2002, at 1430 eastern standard time, a Cessna 172N, N5891E, registered to a private owner and operated by a student pilot, lost directional control during landing and nosed over into a ravine at Cartersville Airport, Cartersville, Georgia. The instructional flight was operated under the provision of Title 14 CFR Part 91 and visual flight rules. Visual meteorological conditions prevailed at the time of the accident. The airplane sustained substantial damage, and the student pilot was not injured. The flight departed McCollum Field, Marietta, Georgia on December 6, 2002 at 1400.

According to the student pilot he was conducting full-stop landings. During the second landing the pilot flared the airplane left of the centerline. When the nose wheel touched down on runway 19 the airplane veered off the left side of the runway. In an attempt to regain control of the airplane the pilot pulled back on the control yoke, and added power. The airplane traveled approximately 50 yards off the runway, nosed over in a ravine, and came to rest inverted.

Examination of the airplane revealed the nose wheel separated from the nose strut. Both wings were buckled on the upper surface of the wing and had stringer damage. The fuselage was buckled under the cabin. Examination of the nose gear steering tube assemblies revealed continuity from the rudder peddles to the nose gear. When rudder pedal input was entered the nose gear steering tube assemblies operated properly. No mechanical or flight control problems were reported by the student pilot before the accident.

Review of the students pilot's logbook revealed .6 hours of solo hours in type of airplane, and 21 hours of total time.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ATL03LA024