N6995Q

Substantial
None

Beech 23S/N: M-1102

Accident Details

Date
Saturday, March 8, 2003
NTSB Number
IAD03LA037
Location
Cincinnati, OH
Event ID
20030312X00322
Coordinates
39.246665, -84.388885
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

The second pilot's inadequate flare and the pilot/owner's lack of remedial action, which resulted in a hard landing. A factor was the wind gusts.

Aircraft Information

Registration
N6995Q
Make
BEECH
Serial Number
M-1102
Engine Type
Reciprocating
Year Built
1968
Model / ICAO
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
KLEINE DOUGLAS A
Address
8269 WOODBINE AVE
Status
Deregistered
City
CINCINNATI
State / Zip Code
OH 45216-1451
Country
United States

Analysis

On March 8, 2003, at 1315 eastern standard time, a Beech 23, N6995Q, was substantially damaged during a landing at Cincinnati - Blue Ash Airport (ISZ), Cincinnati, Ohio. The certificated private pilot/owner, a second pilot, and a passenger were not injured. Visual meteorological conditions prevailed for the flight which originated at Virgil I. Grissom Municipal Airport (BFR), Bedford, Indiana. No flight plan was filed for the personal flight which was conducted under 14 CFR Part 91.

According to the owner of the airplane, he and the second pilot had completed a flight from Cincinnati to Bedford, during which, the owner was seated in the left seat and the second pilot was in the right seat. After landing at Bedford, the airplane was refueled and the pilots changed seats. The owner stated that he remained pilot-in-command during the return flight from Bedford to Cincinnati, even though the second pilot was manipulating the controls.

Upon arrival in Cincinnati, the second pilot entered the traffic pattern and prepared for a landing on runway 24. He added two notches of flaps, and maintained an approach speed of 80 mph as the airplane crossed the runway threshold. About 20 feet above the ground, the second pilot initiated a flare, and the airplane "dropped straight down" and impacted the runway.

The owner reported that the pilots did not obtain a weather briefing or check the winds from the ASOS or AWOS reporting systems on the field, prior to landing. The owner estimated the winds were from 220 degrees at 10-15 knots, gusting to about 20 knots. He also reported no mechanical anomalies with the airplane, and that he had 138 hours of flight experience, with 43 hours in make and model.

The second pilot reported that he intended to "land long" on runway 24, due to the "turbulent wind" on final approach. However, just after crossing the threshold, the airplane "fell straight down," and impacted the runway. The second pilot also stated that the approach speed of the airplane was about 80 mph; however, he felt he should have added more power due to the wind conditions. The second pilot reported 70 hours of flight experience, 6 of which were in make and model.

Examination of the airplane by a Federal Aviation Administration (FAA) inspector revealed substantial damage to both wings, the landing gear, and the propeller.

Weather reported at an airport 9 miles to the south, at 1253, included winds from 190 degrees at 13 knots, 10 miles visibility, and clear skies.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# IAD03LA037