N3629E

Substantial
None

Grumman G-164BS/N: 744B

Accident Details

Date
Friday, May 16, 2003
NTSB Number
SEA03LA086
Location
Basin City, WA
Event ID
20030609X00823
Coordinates
46.590831, -119.212776
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The failure of the torque sensor idler gear duplex bearing during agricultural aerial application, resulting in a total power loss and a forced landing. Factors include tall wheat and soft terrain.

Aircraft Information

Registration
N3629E
Make
GRUMMAN
Serial Number
744B
Engine Type
Turbo-shaft
Model / ICAO
G-164BG64T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
HALEY'S FLYING SERVICE INC
Address
PO BOX 1049
Status
Deregistered
City
TRACY
State / Zip Code
CA 95378-1049
Country
United States

Analysis

On May 16, 2003, approximately 1300 Pacific daylight time, a Grumman G-164B, N3629E, nosed over during a forced landing in a wheat field about five miles west of Basin City, Washington. The commercial pilot, who was the sole occupant, was not injured, but the aircraft, which is owned by Haley's Flying Service, and leased by the pilot, sustained substantial damage. The 14 CFR Part 137 agricultural application flight, which departed a local agricultural airstrip about 15 minutes before the accident, was being operated in visual meteorological conditions.

According to the pilot, who failed to return an NTSB Form 6120.1/2, he had just executed a reversal turn in order to start another spraying swath when the turbine engine suddenly stopped and the propeller feathered. He attempted to land on a road near the edge of the field he was spraying, but a tractor was on the road so he had to land in a crop of tall wheat. Just before touchdown, one of the aircraft's wings impacted the terrain, and during the landing roll on the soft terrain, the aircraft nosed over.

During a post-accident teardown inspection it was determined that the torque sensor idler gear duplex bearing (part number 3103035-1) had failed, which is a condition that would normally result in an uncommanded in-flight shutdown of the engine. Further inspection of the bearing revealed only minimal heat stress discoloration and no clear lack of lubrication, but the bearing balls had been worn undersize, and the bearing cage had fractured into pieces. Further inspection of the bearing by Honeywell Mechanical Systems, reveled that the bearing condition was consistent with advanced rolling contact fatigue failure.

As part of the investigation, an FAA Airworthiness Inspector from the Portland, Oregon, Flight Standards District Office determined that, "The installation of the subject matched bearing set was performed properly by the last overhaul shop in accordance with the Allied-Signal (Honeywell) Overhaul Specification No. 72-00-17, revised July 20, 1992." Although the reason for the unexpected failure of this bearing after approximately 100 hours of operation could not be determined, it was noted that at the last overhaul the Torque Sensor was not upgraded to the available -3 bearing, which uses a larger bearing assembly and a different gear set.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA03LA086