N7938J

Substantial
None

Bell 47 G5S/N: 25043

Accident Details

Date
Sunday, July 6, 2003
NTSB Number
LAX03LA226
Location
Salinas, CA
Event ID
20030722X01168
Coordinates
36.666942, -121.760276
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The failure of a piston connecting rod during an aerial application, which resulted in a total loss of engine power and subsequent forced landing.

Aircraft Information

Registration
N7938J
Make
BELL
Serial Number
25043
Engine Type
Reciprocating
Year Built
1971
Model / ICAO
47 G5B47G
Aircraft Type
Rotorcraft
No. of Engines
1

Registered Owner (Historical)

Name
SALE REPORTED
Address
NONE
Status
Deregistered
City
XXX
State / Zip Code
OK 73125
Country
United States

Analysis

On July 6, 2003, about 1030 Pacific daylight time, a Bell 47 G5, N7938J, made a forced landing following an uncontained engine failure near Salinas, California. During the forced landing, the main rotor flexed downward and severed the tail boom. Gomes Farm Air Service, Inc., was operating the helicopter under the provisions of 14 CFR Part 137. The commercial pilot, the sole occupant, was not injured; the helicopter sustained substantial damage. The local aerial application flight departed Salinas, about 1030. Day visual meteorological conditions prevailed, and no flight plan had been filed. The primary wreckage was at 36 degrees 40 minutes north latitude and 121 degrees 45 minutes west longitude.

The pilot reported he had made several passes during an aerial application flight. While on the downwind leg the engine shuttered violently then quit. The pilot performed a run-on landing. During the landing sequence the main rotor blade made contact with the tail boom of the helicopter severing the tail rotor gearbox. The engine of the helicopter was externally inspected and the aft section of the engine case was ruptured.

The pilot said that they had experienced the same type of failure 3 years ago. The engine on the accident helicopter had 623 hours since last overhaul.

The pilot/owner reported that upon examination of the engine they found brass shavings in the oil and oil filter. The # 3 piston connecting rod had broken in flight which resulted in the total loss of power.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX03LA226