N8199D

Substantial
Serious

Piper PA-28-181S/N: 28-8290115

Accident Details

Date
Sunday, July 20, 2003
NTSB Number
NYC03LA163
Location
Sandusky, OH
Event ID
20030728X01201
Coordinates
41.433334, -82.652221
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
4
Minor Injuries
0
Uninjured
0
Total Aboard
4

Probable Cause and Findings

The pilot's failure to maintain the engine mixture control during the go-around, which resulted in a loss of power, and in-flight collision with trees.

Aircraft Information

Registration
N8199D
Make
PIPER
Serial Number
28-8290115
Engine Type
Reciprocating
Year Built
1982
Model / ICAO
PA-28-181P28A
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
BACK FORTY FLYING CLUB INC
Address
7126 TWELVE OAK CT
Status
Deregistered
City
FORT WAYNE
State / Zip Code
IN 46804-4795
Country
United States

Analysis

On July 20, 2003, about 1050 eastern daylight time, a Piper PA-28-181, N8199D, was substantially damaged during a go-around at the Griffing-Sandusky Airport (SKY), Sandusky, Ohio. The certificated private pilot and three passengers were seriously injured. Visual meteorological conditions prevailed and no flight plan had been filed for the flight that departed Fort Wayne International Airport (FWA), Fort Wayne, Indiana. The personal flight was conducted under 14 CFR Part 91.

The airplane was on approach to runway 27, a 3,559-foot-long, 60-foot-wide, asphalt runway.

The pilot reported that while turning onto the final approach path, he observed a twin-engine airplane on a taxiway near the runway. The pilot was not certain if the airplane was going to utilize the runway, and elected to go-around. The pilot pushed the throttle full-forward and kept his right hand on the power quadrant. The airplane was configured with two notches of flaps during the approach, and the pilot retracted one notch of flaps. The pilot looked over his left shoulder and observed the twin-engine airplane passing under his airplane's left wing, which was approximately 300 feet above the ground, and climbing. The engine then began to "stumble," and he felt the yoke in his left hand becoming very heavy. He looked down at the power quadrant and noticed that the engine mixture control was pulled back. The pilot pushed mixture control in and lowered the airplane's nose to avoid a stall; however, the airplane struck trees about 1/2 mile beyond the departure end of the runway.

The wreckage was moved to a hangar at SKY, where it was examined under the supervision of a Federal Aviation Administration (FAA) inspector. The examination did not revealed any pre-impact malfunctions of the engine and associated controls. The engine was rotated by hand and thumb compression was obtained on all cylinders. All spark plugs were removed. Their electrodes were intact and light gray in color. The right magneto generated a spark through all four of its leads when rotated. The left magneto sustained impact damage and could not be tested. The engine driven fuel pump and carburetor were disassembled with no discrepancies noted.

The pilot reported 338 hours of total flight experience, which included 67 hours in the same make and model airplane as the accident airplane.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# NYC03LA163