N7615Z

Substantial
None

Piper PA-18-150S/N: 18-8398

Accident Details

Date
Monday, September 1, 2003
NTSB Number
NYC03LA187
Location
Midland, VA
Event ID
20030905X01466
Coordinates
38.633888, -77.757225
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

Loss of engine power due to unknown circumstances.

Aircraft Information

Registration
Make
PIPER
Serial Number
18-8398
Engine Type
Reciprocating
Year Built
1966
Model / ICAO
PA-18-150PA18
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
PA-18-150

Registered Owner (Current)

Name
ROBINSON NORMAN D II
Address
2573 SAGE WAY
City
SALT LAKE CITY
State / Zip Code
UT 84109
Country
United States

Analysis

On September 1, 2003, at 1830 eastern daylight time, N7615Z, a Piper PA-18-150, was substantially damaged during a forced landing, following a loss of engine power in Midland, Virginia. The certificated private pilot was not injured. Visual meteorological conditions prevailed and no flight plan was filed for the flight which originated at the Horse Feathers Airport (53VA), Midland, Virginia. The local personal flight was conducted under 14 CFR Part 91.

In a written statement, the pilot reported that the accident flight was the airplane's first flight since the engine had undergone a field overhaul.

According to the pilot, after flying for about 1 hour 15 minutes, while in cruise flight, the engine lost power. The airplane was at an altitude of 1,600-1,700 feet msl, and about 1 mile from the departure airport. As the pilot prepared for a forced landing, he realized that the airplane would not be able to make it to the airport, and he attempted a forced landing to a field. The pilot extended full flaps while on final approach, and the airplane touched down at the mid-point of the field. During the landing rollout, the pilot applied right rudder to stay aligned with the field, and the airplane nosed-over.

The pilot reported that all preflight and in-flight engine indications appeared normal prior to the loss of engine power. At the time of the power loss, the left fuel tank gauge indicated 1/8-full, and the right fuel tank gauge, which had been selected for the entire flight, indicated just less than 1/4-full. The pilot departed with approximately 15 gallons of fuel for the flight.

The on-scene examination of the airplane by a Federal Aviation Administration (FAA) inspector revealed no obvious pre-impact mechanical malfunctions. The inspector was unable to visually inspect the fuel tanks due to the inverted position of the airplane; however, the surrounding vegetation in the area of the fuel tanks appeared discolored and had an odor consistent with aviation fuel. During the recovery of the airplane, it was noted that "little" fuel was left in the fuel tanks; however, the fuel vent system consisted of drilled holes in the fuel tank caps.

The engine was test run on the airframe, using its own fuel system. The engine started and ran at various power settings for several minutes, with no abnormalities noted.

According to the Piper PA-18 Owner's Handbook, the fuel consumption for the airplane was 9 gallons per hour.

Weather reported at the Manassas Regional Airport, located about 12 miles to the northeast of the accident site, at 1836, included wind from 160 degrees at 6 knots, 10 miles visibility, clear skies, temperature 82 degrees Fahrenheit, dew point 73 degrees Fahrenheit, and barometric pressure setting of 30.08 inches Hg.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# NYC03LA187