N258HB

Substantial
None

Kucklick HiperbipeS/N: 258

Accident Details

Date
Saturday, August 23, 2003
NTSB Number
NYC03CA182
Location
Marion, OH
Event ID
20030915X01542
Coordinates
40.619445, -83.053337
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The pilot's improper decision to install an inadequate air filter, which subsequently failed and resulted in a power loss.

Aircraft Information

Registration
N258HB
Make
KUCKLICK
Serial Number
258
Engine Type
Reciprocating
Year Built
1989
Model / ICAO
HiperbipeSA02
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
CONRY MICHAEL A
Address
4796 S OURAY ST
Status
Deregistered
City
AURORA
State / Zip Code
CO 80015-1743
Country
United States

Analysis

On August 23, 2003, about 1430 eastern daylight time, a homebuilt Hyperbipe, N258HB, was substantially damaged following a loss of engine power while departing Marion Municipal Airport, Marion, Ohio. The certificated private pilot and passenger were not injured. Visual meteorological conditions prevailed for the personal flight destined for Beaver County Airport, Beaver Falls, Pennsylvania. No flight plan had been filed for the flight that was conducted under 14 CFR Part 91.

The pilot reported that the airplane lost engine power during the initial climb after takeoff. He further stated:

"...At approx 250 to 400 feet of altitude, the engine began to loose power slowly. I could not climb or maintain altitude due to the steady loss of power and began to sink rapidly. I picked a field I thought I could make an emergency landing on straight ahead. I pulled the throttle to idle and pulled the mixture to cut off just before touch down as I flared for a landing in a farm field of soy beans. With no injuries to my self or passenger, we exited the plane as quickly as possible...."

During a follow-up telephone interview, the pilot reported that from the air, he thought the height of the vegetation in the field he had picked for a landing was about 6 inches; however, it turned out be about 40 inches high.

A mechanic who examined the airplane reported that the air filter screen had separated from the support bracket. The filter element was found in the intake to the fuel injection servo and obstructed the air flow to the engine. The mechanic said he had given the airplane a condition inspection about 30 hours before the accident, and an air filter was not installed at that time. The air filter was "home-made" and installed by the pilot. The filter screen was attached to the support bracket by the use of pop rivets.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# NYC03CA182