N73179

Substantial
None

Cessna 172MS/N: 17267306

Accident Details

Date
Sunday, September 14, 2003
NTSB Number
LAX03CA288
Location
Tucson, AZ
Event ID
20031021X01789
Coordinates
32.123332, -110.947776
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

the pilot's improper flare. A contributing factor was the tailwind.

Aircraft Information

Registration
Make
CESSNA
Serial Number
17267306
Engine Type
4-cycle
Model / ICAO
172MC172
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
172M

Registered Owner (Current)

Name
WEENGKNUTTS 179
Address
1834 N SUNSET DR
City
DELTA
State / Zip Code
UT 84624-7480
Country
United States

Analysis

On September 14, 2003, at 1238 mountain standard time, a Cessna 172M, N73179, made a hard landing and collapsed the nose landing gear at Tucson International Airport (TUS), Tucson, Arizona. Arizona Aero Tech was operating the airplane under the provisions of 14 CFR Part 91. The private pilot, the sole occupant, was not injured; the airplane sustained substantial damage. Visual meteorological conditions prevailed and a flight plan had not been filed.

The pilot reported in a written statement that he was practicing touch-and-go takeoffs and landings on runway 11R. He recalled the automated terminal information service (ATIS) was reporting winds from 180 at 4 knots. The takeoff was uneventful. He turned onto final and noted he was slightly below a normal glide path, as indicated by the precision approach path indicator lights (PAPI). He leveled out to correct and continued on final, with the flaps extended to a 40-degree setting.

Approximately 5 feet above the runway, the pilot felt a higher than normal sink rate. He applied full power; however, the airplane contacted the runway and bounced. He increased power in a go-around attempt, and the airplane drifted to the left side of the runway. It gained altitude and he retracted "a little bit" of the flaps. The airplane then impacted the ground. The pilot reported flying about 2 hours in the past 90 days preceding the accident.

In a phone conversation, the pilot reported to the Safety Board investigator-in-charge (IIC) that after making the final impact with the runway, the nose gear collapsed and the airplane skidded on its nose. He felt the accident was the result of the airplane being at too slow of airspeed on final and his delayed reaction.

A routine aviation weather report (METAR) was issued at 1235. It reported winds from a magnetic bearing of 330 degrees at 4 knots.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX03CA288