N239HL

Substantial
None

Avions Max Holste MH 1521 BROUSSARD S/N: 239

Accident Details

Date
Saturday, October 11, 2003
NTSB Number
LAX04CA010
Location
El Cajon, CA
Event ID
20031112X01889
Coordinates
32.826110, -116.972503
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

the pilot's premature liftoff and his failure to attain an adequate takeoff airspeed, which resulted in a stall. The pilot's failure to correctly set the pitch trim before takeoff was a factor.

Aircraft Information

Registration
N239HL
Make
AVIONS MAX HOLSTE
Serial Number
239
Engine Type
Reciprocating
Year Built
1960
Model / ICAO
MH 1521 BROUSSARD BROU
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
CHAFFIN GENE E
Address
17270 OLD YUCCA TRL
Status
Deregistered
City
ESCONDIDO
State / Zip Code
CA 92027-6609
Country
United States

Analysis

On October 11, 2003, about 1145 Pacific daylight time, an Avions Max Holste MH 1521 Broussard, N239HL, stalled during takeoff from Gillespie Field (SEE), El Cajon, California. The pilot was operating the airplane under the provisions of 14 CFR Part 91. The private pilot and three passengers were not injured; the airplane sustained substantial damage. Visual meteorological conditions prevailed, and a visual flight rules flight plan had been filed. The personal flight, en route to San Felipe, Mexico, was originating at the time of the accident.

In a written statement the pilot reported that he was number 3 for takeoff, with seven airplanes waiting behind him. He did an expedited takeoff, rather than his usual takeoff procedures of lining up on the centerline and releasing the brakes after reaching 2,500 rpm. The initial takeoff roll was normal. After approximately 3 seconds, the pilot applied forward stick to raise the tail. After 5 seconds, the tail was still on the ground. He then moved his left hand to the stick so that he could use his right hand to apply nose down trim. However, before he could apply it, the airplane ballooned about 8 feet into the air. As it recontacted the ground, the airplane bounced, and the right wing stalled. The right wing impacted the ground, followed by the left main gear, and then the left wing tip. The propeller contacted the ground as the left main gear hit, and the engine stopped. The pilot did not report any mechanical problems with the airplane and reported that "additional nose down trim" could have prevented the accident.

In a telephone conversation, the pilot reported that he took off prior to reaching takeoff airspeed and stalled the airplane.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX04CA010