N9374H

Substantial
None

Cessna 182RS/N: 18267939

Accident Details

Date
Thursday, January 22, 2004
NTSB Number
FTW04LA064
Location
Ringgold, TX
Event ID
20040126X00107
Coordinates
33.849445, -97.945274
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilots failure to maintain clearance from the support wire while on a pipeline patrol flight. A contributing factor was the haze restricting the pilots forward visibility, and low altitude flight.

Aircraft Information

Registration
Make
CESSNA
Serial Number
18267939
Engine Type
Reciprocating
Year Built
1981
Model / ICAO
182RC182
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
182R

Registered Owner (Current)

Name
BARR AIR PATROL LLC
Address
1442 AIRPORT BLVD # 11
City
MESQUITE
State / Zip Code
TX 75181-1339
Country
United States

Analysis

On January 22, 2004, approximately 0950 central standard time, a Cessna 182R single-engine airplane, N9374H, was substantially damaged upon impacting a support wire for a tower near Ringgold, Texas. The commercial pilot, sole occupant of the airplane, was not injured. The airplane was registered to United Helicopters Incorporated DBA and operated by the Barr Patrol of Mesquite, Texas. Visual meteorological conditions prevailed and a company flight plan was filed for the 14 Code of Federal Regulations Part 91 aerial observation flight. The cross-country flight originated from the Mesquite Metro Airport (HQZ), near Mesquite, Texas, at 0820, and was destined to the Guymon Municipal Airport (GUY), near Guymon, Oklahoma.

The 16,000-hour pilot reported in the Pilot/Operator Aircraft Accident Report (NTSB Form 6120.1/2) that he was flying on a pipeline patrol 1.5 miles north of Ringgold, Texas, on a heading of 335 degrees. He further reported that the weather was "clear but with a gray haze to the north." With the prevailing weather conditions, the pilot stated that the unlit tower was hard to see, and "by the time I saw it, it was too late to take evasive action."

During a telephone interview, conducted by the NTSB investigator-in-charge (IIC), the pilot reported the airplane was at an altitude of 300 feet agl and shortly after impact with the "support wire," he "deemed the airplane flyable and proceeded to evaluate its maneuverability." He climbed to 2,500 msl and slowed the airplane down to 60 knots and assessed the controllability in a landing configuration. The pilot then elected to return to HQZ.

Examination of the airplane by the pilot revealed that the outboard 18 inches of the right wing was severed. The pilot stated, "I couldn't see the extent of the wing damage from where I was sitting."

The unlit tower was depicted on the sectional chart.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW04LA064