N7736K

Substantial
None

Cessna P210NS/N: P21000420

Accident Details

Date
Tuesday, July 20, 2004
NTSB Number
DEN04LA107
Location
Douglas, WY
Event ID
20040726X01068
Coordinates
42.749061, -105.390792
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
4
Total Aboard
4

Probable Cause and Findings

the failure of the engine's crankshaft due to the rotation of the engine's number two bearing, which resulted in the oil starvation of the crankshaft's number 2 main journal. Contributing factors include the engine's improper maintenance, and the in-flight collision with a fence post during a forced landing.

Aircraft Information

Registration
Make
CESSNA
Serial Number
P21000420
Engine Type
Reciprocating
Year Built
1979
Model / ICAO
P210NC210
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
6
FAA Model
P210N

Registered Owner (Current)

Name
VALIAIR LC TRUSTEE
Address
OGDEN AIRPORT GATEWAY CENTER
4248 S 1650 E BLDG 1 STE 10
City
OGDEN
State / Zip Code
UT 84405
Country
United States

Analysis

On July 20 2004, at 1600 mountain daylight time, a Cessna P210N, N7736K, operated by a commercial pilot, was substantially damaged during a forced landing at Converse County Airport (DGW), Douglas, Wyoming. Visual meteorological conditions prevailed at the time of the accident. The personal cross-country flight was being conducted under the provisions of Title 14 CFR Part 91 on an instrument flight rules (IFR) flight plan. The pilot and three passengers were not injured. The flight to Provo, Utah, originated at Rapid City, South Dakota, approximately 1400.

According to the pilot, while in cruise flight at 22,000 feet msl, the engine "quit." The pilot stated that the propeller continued to "windmill," and at that time he noted approximately 50 gallons of fuel remaining. The pilot's attempts to restart the engine were unsuccessful. He declared an emergency and was diverted to Douglas. He broke out of the clouds at approximately 14,000 feet agl. On final approach to runway 28, the airplane's left main landing gear struck a fence post and the airplane impacted terrain approximately 200 feet short of the runway threshold. The airplane drifted to the left of the runway centerline and came to a stop in the grass. The impact collapsed the airplane's left main landing gear assembly, and buckled the left wing tip and left horizontal stabilizer.

On February 14, 2005, the engine was examined at Teledyne Continental Motors, Inc., in Mobile, Alabama. The examination revealed a 7/8-inch by 3/8-inch hole in the top of the crankcase, just forward of the number 1 cylinder. Further examination revealed that the number 2, 3, 4, 5, and 6 piston rods were fractured. The engine crankshaft was fractured at the number 2 rod journal. The crankshaft exhibited thermal discoloration and impact marks at the number 2, 3, 4, and 5 rod journals. Rotational scoring and thermal discoloration was observed on each main bearing. The crankshaft's number 2 main bearing was fragmented. Fretting was observed on the crankcase halves at the number 2 bearing through bolts. Fretting was also observed on the number 3 and 4 bearing through bolts.

According to the airplane's engine maintenance records, on May 31, 2000, at an airframe total time of 2,380.0 hours, a top overhaul was completed on all 6 cylinders. On November 17, 2003, at 2,845.0 hours, during the airplane's most recent 100-hour inspection, the engine's number 2 cylinder was replaced. At the time of the accident, the total airframe time was 3,083.0 hours.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# DEN04LA107