Summary
On August 15, 2004, a Cessna 182S (N537CR) was involved in an incident near Eastport, MI. All 3 people aboard were uninjured. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this incident to be: The pilot misjudging the landing flare resulting in the hard landing and his unsuccessful remedial action following the bounced landing.
On August 15, 2004, about 0900 eastern daylight time, a Cessna 182S, N537CR, piloted by a private pilot, sustained substantial damage when the nose landing gear collapsed during landing on runway 27 (3,300 feet by 100 feet, turf), at the Torchport Airport, Eastport, Michigan. The 14 CFR Part 91 personal flight was operating in visual meteorological conditions without a flight plan. The pilot and two passengers were not injured. The flight originated from Grosse Isle, Michigan about 0700.
In a written statement, the pilot stated that during landing, the airplane settled to the ground and then bounced about 2 feet into the air. He stated that airplane came back down and the nose wheel impacted a small depression in the airstrip.
This incident is documented in NTSB report CHI04LA232. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N537CR.
Accident Details
Probable Cause and Findings
The pilot misjudging the landing flare resulting in the hard landing and his unsuccessful remedial action following the bounced landing.
Aircraft Information
Registered Owner (Historical)
Analysis
On August 15, 2004, about 0900 eastern daylight time, a Cessna 182S, N537CR, piloted by a private pilot, sustained substantial damage when the nose landing gear collapsed during landing on runway 27 (3,300 feet by 100 feet, turf), at the Torchport Airport, Eastport, Michigan. The 14 CFR Part 91 personal flight was operating in visual meteorological conditions without a flight plan. The pilot and two passengers were not injured. The flight originated from Grosse Isle, Michigan about 0700.
In a written statement, the pilot stated that during landing, the airplane settled to the ground and then bounced about 2 feet into the air. He stated that airplane came back down and the nose wheel impacted a small depression in the airstrip. He said that he held the nose off of the ground for about another 60 to 100 yards before the airplane settled onto the engine cowl.
The airplane sustained damage to the propeller, engine, engine mount, firewall and fuselage.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI04LA232