N5157T

Destroyed
Fatal

Cessna R182S/N: R18201826

Accident Details

Date
Thursday, September 23, 2004
NTSB Number
MIA04FA128
Location
Milton, FL
Event ID
20040929X01515
Coordinates
30.645277, -86.998611
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
4
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
4

Probable Cause and Findings

The pilots operation of the airplane with known deficiencies in the equipment based on witness statements describing an excessive rpm drop and rough running engine after starting, during the engine run-up, and after becoming airborne, his failure to abort the takeoff after an excessive takeoff roll, and his failure to maintain airspeed resulting in an inadvertent stall, uncontrolled descent, and in-flight collision with terrain. A factor in the accident was the loss of engine power due to undetermined reasons.

Aircraft Information

Registration
N5157T
Make
CESSNA
Serial Number
R18201826
Engine Type
Reciprocating
Year Built
1981
Model / ICAO
R182C82R
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
PROPCO INC
Address
204 ROCHESTER RD
Status
Deregistered
City
MOBILE
State / Zip Code
AL 36608-2219
Country
United States

Analysis

HISTORY OF FLIGHT

On September 23, 2004, about 1006 central daylight time, a Cessna R182, N5157T, registered to PropCo, Inc., operated by MC Aviation, Inc., experienced an in-flight loss of control and crashed in a residential area located .30 nautical mile west-northwest from the departure end of runway 36 at Peter Prince Field Airport, Milton, Florida. Visual meteorological conditions prevailed at the time and no flight plan was filed for the 14 CFR Part 91 local, personal flight from Peter Prince Field Airport. The airplane was destroyed by impact and a postcrash fire and the commercial-rated pilot and three passengers were fatally injured. The flight originated about 5 minutes earlier from Peter Prince Field Airport.

An acquaintance of the pilot reported the purpose of the flight was to survey damage to the church in which he and the passengers were members of, to survey damage to the homes of church members, and to survey the area in general as a result of Hurricane Ivan to see where assistance from the church was needed.

One witness reported seeing four adults board the airplane and three separate witnesses reported hearing the pilot have a difficult time starting the engine, then after it was started, all three reported hearing the engine running "rough." One of the witnesses is a FAA certificated airframe and powerplant (A & P) mechanic. The airplane was observed taxiing to the approach end of runway 36 and one of the three witnesses reported, "During the run up his mag check sounded like it had excessive drop. He increased rpm's and held it there." The witness who is an A & P mechanic reported, "They taxied to the run-up area and in my opinion had an unsatisfactory pre-flight run-up/test. Evidently they chose to take off with the poorly running engine." The third witness reported, "...Got to the runway to do a run up. [Magneto] check sounded rough...."

The airplane was taxied onto the 3,700 foot long runway and began the takeoff roll but one of the witnesses reported the engine was, "making sounds as if it was not developing power." The A & P mechanic and one other witness reported the airplane became airborne when it was approximately 3/4 down the runway. The A & P mechanic stated, "The aircraft used 3/4 of the runway trying to get airborne and never developed full power. I would estimate they achieved 100 feet of altitude...." One witness reported seeing the landing gear retract after the airplane became airborne, while another witness reported hearing a rough running engine when the airplane flew overhead her position.

A pilot-rated witness who was airborne at the time of the accident reported seeing the flight depart from runway 36. The pilot-rated witness further reported that, "after he had turned downwind the airplane appeared to stall, then pitch straight down." He discontinued his approach, circled the crash site, observed fire, and advised FAA air traffic control of the accident.

PERSONNEL INFORMATION

The pilot was the holder of a commercial pilot certificate with airplane single engine land, airplane multi-engine land, and instrument airplane ratings. His commercial pilot certificate was first issued on January 27, 1999. The certificate issued on that date had airplane single engine land and instrument airplane ratings. He was issued a first class medical certificate on March 23, 2004, with the restriction, "must wear corrective lenses."

A review of copies of his pilot logbooks that contained entries from his first flight on December 14, 1996, to the last entry dated March 7, 2002, revealed no logged flights in the accident make and model airplane. He logged a total time of 2,046.6 hours, 519.1 hours in airplane single engine land airplanes, and 1,482.4 in airplane multi-engine land airplanes. He also logged 647.6 hours as pilot-in-command, and 1,357.8 hours as second-in-command. Further review of his pilot logbook revealed the remarks section of an entry dated January 5, 2001, indicating "Hired at Continental [Express] Part 121." From that date (January 5, 2001), to the last entry in the logbook (March 7, 2002), he logged only 1 flight in a general aviation airplane. That flight occurred on August 3, 2001, the duration was 1.0 hour, and the remarks section for that entry indicates, "Aircraft [check] out PA28-161."

According to FAA records, the right front seat occupant was not a certificated pilot.

AIRCRAFT INFORMATION

The airplane was manufactured in 1981 by Cessna Aircraft Company as model R182, and was designated serial number R18201826. It was certificated in the normal category and was equipped with a Textron Lycoming O-540-J3C5D engine rated at 235 horsepower when operated at 2,400 rpm. The airplane was also equipped with a McCauley B3D32C407-B constant speed propeller.

Review of the airplane maintenance records revealed the airplane was last inspected in accordance with a 100-Hour inspection on August 16, 2004. At that time the airplane had accumulated 3,150.0 hours total time. The airplane had accumulated 40.3 hours since the inspection at the time of the accident.

Further review of the maintenance records revealed the engine was overhauled by Don George, Inc., in November 1992, and installed in the airplane following overhaul on December 11, 1992. The engine was removed from the airplane due to a propeller strike, disassembled and inspected in October 1993. The engine was reinstalled in the airplane on October 27, 1993, and remained installed until removed postaccident. On August 16, 2004, an entry in the engine logbook indicates in part, "all cylinders were removed and overhauled by John Jewel Aircraft CRS JUJR300L, due to exhaust flange erosion." At the time of the accident the engine had accumulated 920 hours since major overhaul, and approximately 40 hours since the overhauled cylinders were installed.

METEOROLOGICAL INFORMATION

A surface observation weather report taken at the Pensacola Regional Airport (KPNS), Pensacola, Florida, on the day of the accident at 0953, or approximately 13 minutes before the accident indicates the wind was from 080 degrees at 9 knots, clear skies existed, the temperature and dew point were 24 and 18 degrees Celsius, respectively, and the altimeter setting was 30.14 inHg. The accident site was located approximately 14 nautical miles and 045 degrees from KPNS.

AIRPORT INFORMATION

The Peter Prince Airport is equipped with one asphalt runway designated 36/18, which is 3,700 feet in length by 75 feet wide. The airport elevation is 82 feet, and the airport is equipped with a common traffic advisory frequency (CTAF)/UNICOM of 122.975 mHz, that is not recorded.

WRECKAGE AND IMPACT INFORMATION

The airplane crashed in the sideyard of a house located at 7732 Erudition Avenue, Milton, Florida. The accident site was located at 30 degrees 38.721 minutes North latitude and 086 degrees 59.911 minutes West longitude, or approximately .30 nautical mile and 303 degrees magnetic from the departure end of runway 36. The accident site was located .61 statute mile and 333 degrees from the center of the airport.

Examination of the accident site revealed the wreckage was upright on a magnetic heading of 035 degrees magnetic near a lake. The engine assembly was beneath ground level with only the outer 10 inches of one propeller blade visible. The "backbone" of the engine was at an angle of approximately 40 degrees with respect to the nearly level ground. The smell of 100 low lead fuel was noted in the ground while digging the earth away from the engine. Fire damage to grass was noted surrounding the left wing, fuselage, empennage, aft portion of the right wing, and at the right wingtip resting location.

Examination of the airplane revealed the fuselage was consumed by the postcrash fire from the instrument panel aft to approximately 6 inches forward of the leading edge of the horizontal stabilizer, and fire damage was noted to both wings. Fire damage was also noted to both horizontal stabilizers, the vertical stabilizer, the left elevator, and to a portion of the rudder. Slight paint discoloration was noted on the inboard leading edge and inboard upper skin of the right elevator. All components necessary to sustain flight remained attached to the airplane or were in close proximity to the main wreckage. Bulging of the upper wing skins of both wings consistent with hydraulic deformation was noted in the areas where the fuel tank was installed. Flight control continuity was confirmed for pitch and yaw. Examination of the aileron flight control system revealed both primary flight control cables were fractured near each wing root area; the cables were fractured in tension overload. The aileron balance cable was continuous from the left aileron bellcrank to the right aileron bellcrank. The propeller remained secured to the engine which remained secured to the airframe. One propeller blade was separated from the propeller hub but was found in the engine impact crater. The flaps were retraced based on the examination of the flap actuator, and the landing gear was retracted.

Examination of the fuel system revealed the outlet screens of the left and right fuel tanks were free of obstructions. The fuel line from the left fuel tank to the fuel selector was compromised in several locations due to fire, and the fuel line from the right fuel tank was noted going down the aft door post but was not connected in the wing root area due to an excessive gap at the right wing root. The crossover vent line was free of obstructions. The fuel selector was free of obstructions. No obstructions were noted in any fuel line from the fuel selector valve to carburetor inlet fitting. The fuel strainer screen was clean. Vented fuel caps were installed on both fuel tanks. The auxiliary fuel pump was removed for further examination.

Examination of the cockpit revealed the mixture, throttle, and carburetor heat controls were f...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA04FA128