N6535K

Substantial
None

Grumman G-164CS/N: 3C

Accident Details

Date
Sunday, May 8, 2005
NTSB Number
LAX05LA165
Location
Willows, CA
Event ID
20050513X00612
Coordinates
39.516387, -122.217498
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

the loss of engine power due to the fractured piston pin boss on the number 5 cylinder.

Aircraft Information

Registration
Make
GRUMMAN
Serial Number
3C
Engine Type
Reciprocating
Year Built
1977
Model / ICAO
G-164CG64T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
1
FAA Model
G-164C

Registered Owner (Current)

Name
JONES AVIATION INC
Address
PO BOX 497
City
BIGGS
State / Zip Code
CA 95917-0497
Country
United States

Analysis

On May 8, 2005, at 0916 Pacific daylight time, a restricted category Grumman G-164C, N6535K, force landed in a rice field after a loss of engine power near Willows, California. Chuck Jones Flying Service, who was also the registered owner of the airplane, was operating it under the provisions of 14 CFR Part 137. The commercial pilot was not injured; the airplane sustained substantial damage. Visual meteorological conditions prevailed and no flight plan was filed for the local area agricultural application flight.

According to the pilot, while seeding rice over a field, the engine lost partial power. The pilot force landed the airplane in a field. During the landing roll, the landing gear impacted a berm and were sheared from their structural attachment points on the airplane. Until the ground impact, the engine was producing partial power, but not enough to sustain flight.

The Federal Aviation Administration accident coordinator reported that the number 5 cylinder piston had fractured at the piston pin boss. The piston pin, which is mounted in the piston pin boss and holds the piston to the connecting rod, fell from the boss and the connecting rod was free to rotate. Following the accident, the piston was jammed in the cylinder barrel and had to be cut from the engine for removal. The engine was overhauled about 1,154 hours prior to the accident. The maintenance history on the piston could not be determined based on available records.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX05LA165