Summary
On May 30, 2005, a Cessna 182F (N3225U) was involved in an incident near Osage Beach, MO. All 4 people aboard were uninjured. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this incident to be: The pilot's improper flare and his inadequate recovery from the bounced landing which resulted in a hard landing. A factor associated with the accident was the improper landing flare.
On May 30, 2005, at 1600 central daylight time, a Cessna 182F, N3225U, experienced a hard landing on runway 14 (3,205 feet by 60 feet, asphalt) at the Grand Glaize Airport (K15), Osage Beach, Missouri. The private pilot and three passengers were not injured. The airplane received substantial damage. The 14 Code of Federal Regulations Part 91 personal flight was operating in visual meteorological conditions without a flight plan. The local flight originated from K15 at 1530.
The pilot stated that upon returning to the airport the winds were reported over the UNICOM frequency as being calm, so he entered the he entered the traffic pattern for runway 14. He stated he that he was too high during this landing attempt so he initiated a go-around.
This incident is documented in NTSB report CHI05CA132. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N3225U.
Accident Details
Probable Cause and Findings
The pilot's improper flare and his inadequate recovery from the bounced landing which resulted in a hard landing. A factor associated with the accident was the improper landing flare.
Aircraft Information
Registered Owner (Current)
Analysis
On May 30, 2005, at 1600 central daylight time, a Cessna 182F, N3225U, experienced a hard landing on runway 14 (3,205 feet by 60 feet, asphalt) at the Grand Glaize Airport (K15), Osage Beach, Missouri. The private pilot and three passengers were not injured. The airplane received substantial damage. The 14 Code of Federal Regulations Part 91 personal flight was operating in visual meteorological conditions without a flight plan. The local flight originated from K15 at 1530.
The pilot stated that upon returning to the airport the winds were reported over the UNICOM frequency as being calm, so he entered the he entered the traffic pattern for runway 14. He stated he that he was too high during this landing attempt so he initiated a go-around. The pilot stated he extended his final approach during the next landing attempt. He stated the approach looked good, but he "misjudged the flare and porpoised several times." The pilot stated he realized the airplane was damaged when he heard a clicking sound while using the right rudder pedal.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI05CA132