N134US

Substantial
Serious

Clarke YAK 3UR 2000S/N: DMC0003

Accident Details

Date
Saturday, July 9, 2005
NTSB Number
DEN05LA106
Location
Heber City, UT
Event ID
20050713X00999
Coordinates
40.481945, -111.428886
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
1
Uninjured
0
Total Aboard
2

Probable Cause and Findings

loss of engine power due to a leaking carburetor and an inoperative float, and the pilot's failure to maintain aircraft control during the restart attempt. Contributing factors were the sudden engine power surge during the attempted restart, and unsuitable terrain on which to make a forced landing.

Aircraft Information

Registration
Make
CLARKE
Serial Number
DMC0003
Engine Type
Reciprocating
Model / ICAO
YAK 3UR 2000
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
YAK 3UR 2000

Registered Owner (Current)

Name
HOLBROOK MASLEN
Address
548 HUBLER LN
City
CALDWELL
State / Zip Code
ID 83605
Country
United States

Analysis

On July 9, 2005, at 0915 mountain daylight time, a YAK 3UR 2000, N134US, piloted by a airline transport pilot, sustained substantial damage when it impacted terrain during a forced landing near Heber City Airport, Heber City, Utah. Visual meteorological conditions prevailed at the time of the accident. The local personal flight was being conducted under the provisions of Title 14 CFR Part 91 without a flight plan. The pilot and passenger sustained minor injuries. The flight originated in Caldwell, Idaho, and was destined for Heber City, Utah.

In a telephone interview, the pilot said that when he turned downwind, the engine lost power. When he attempted to restart the engine, it surged and the torque caused the airplane to roll inverted. The pilot managed to roll the airplane upright, but was unable to restart the engine. He said he "planted" the airplane on the ground. The airplane "bounced ten times" and came to rest 200 to 250 yards from the initial impact point. The engine was torn away from the fuselage.

The carburetor was examined at Precision Engines Corporation in Everett, Washington, and a report issued. The report noted that the enrichment cover was leaking, and there was "a substantial leak" at one of the vapor vent ports. One of the vapor vent floats "does not appear to be functioning correctly," the report said. The vapor vent port was plugged and the carburetor was functionally tested. The carburetor tested between 7 and 22 pounds per hour above the rich limit on test points 1 through 16. All other test points were within limits, as was the automatic mixture control.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# DEN05LA106