N1UH

Substantial
None

Parkwood Enterprises, Inc Glasair Super II-SS/N: 2227

Accident Details

Date
Thursday, June 2, 2005
NTSB Number
DFW05LA153
Location
Los Fresnos, TX
Event ID
20050719X01052
Coordinates
25.906389, -97.425834
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A blocked fuel line in the fuel tank, which resulted in a loss of engine power due to fuel starvation.

Aircraft Information

Registration
Make
PARKWOOD ENTERPRISES, INC
Serial Number
2227
Engine Type
Reciprocating
Year Built
1994
Model / ICAO
Glasair Super II-SBPAT
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
STRD HMLTN SUPER IIS

Registered Owner (Current)

Name
R N D MOTORSPORTS LLC
Address
6458 OLD TAFT RD
City
DULUTH
State / Zip Code
MN 55803-9383
Country
United States

Analysis

On June 2, 2005, at 0750 central daylight time, a single-engine Parkwood Enterprises, Inc, Glasair Super II-S experimental airplane, N1UH, was substantially damaged during a forced landing following a loss of engine power during take off from a private airstrip near Los Fresnos, Texas. The commercial pilot, sole occupant of the airplane, was not injured. The airplane was registered to, and operated by a private company. Visual meteorological conditions prevailed and no flight plan was filed for the personal flight conducted under 14 Code of Federal Regulations Part 91.

In a written statement, the pilot stated that prior to departure, he checked all of the flight instruments, cycled the propeller, checked the magnetos and engine gauges. All checks were normal. The pilot then applied full power and proceeded to take-off from Runway 32. He said that as soon as the airplane became airborne, the engine stopped producing power and it descended and struck a fence before coming to rest in the upright position. The pilot reported that the wings, undercarriage, and right elevator sustained structural damage. The landing gear and propeller were also damaged.

The airplane, which had accumulated a total of 552.8 hours since new, was powered by a 180-horsepower Lycoming IO-360 engine. Examination of the aircraft fuel system by an FAA certificated airframe and powerplant mechanic revealed the fuel injector screen was absent of debris. When the fuel line between the fuel pump and fuel injection servo was removed, little to no fuel was found in the lines. There was no fuel in the fuel injector or in the line between the fuel boost pump and the engine driven fuel pump. In addition, there was no fuel in the hose between the flow divider and the fuel injector servo. Further examination revealed a blockage between the connector in the fuel tank to the engine driven fuel pump.

The pilot reported a total flight time of 5,669.5 hours, of which, 552.8 hours were in same make and model. He also reported that at the time of the accident, the winds were calm.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# DFW05LA153