N5495

Substantial
None

Grumman G-164AS/N: 1029

Accident Details

Date
Monday, August 1, 2005
NTSB Number
NYC05LA126
Location
Felton, DE
Event ID
20050804X01154
Coordinates
39.012779, -75.533607
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The mechanic's inadequate annual inspection, and failure to comply with an airworthiness directive, which resulted in a total failure of the second stage turbine rotor.

Aircraft Information

Registration
N5495
Make
GRUMMAN
Serial Number
1029
Engine Type
Turbo-shaft
Year Built
1973
Model / ICAO
G-164AG64T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
FINUP SPRAYING SERVICE INC
Address
7175 KENDAVILLE RD
Status
Deregistered
City
LAKEVIEW
State / Zip Code
MI 48850-9563
Country
United States

Analysis

On August 1, 2005, about 0940 eastern daylight time, a Grumman G-164A, N5495, was substantially damaged during a forced landing, following a total loss of engine power while maneuvering near Felton, Delaware. The certificated commercial pilot was not injured. Visual meteorological conditions prevailed, and no flight plan was filed for the local aerial application flight conducted under 14 CFR Part 137.

The pilot stated that he was returning to a private airstrip after a 25-minute aerial application flight. The airplane was about 500 feet agl, when the pilot heard a loud explosion from the engine. The pilot immediately began looking for a suitable field to perform an emergency landing. He then observed a soybean field, and initiated a right turn in an attempt to glide to the field. The airplane was descending rapidly, and before the pilot could level the wings, the right wing contacted the ground. The airplane subsequently bounced hard on the main gear and came to rest inverted.

The airplane was equipped with a Honeywell (Garrett) TPE331-43A turboprop engine. Initial examination of the engine by a Federal Aviation Administration (FAA) inspector revealed that the second stage turbine rotor had separated. The engine was subsequently disassembled and inspected at the manufacturer's facility, under the supervision of an FAA inspector. The inspector noted that the second stage turbine rotor was fractured, separated, and lodged in the back of the engine. The second stage turbine stator seal plate assembly exhibited warpage. In addition, the forward face of the second stage turbine rotor exhibited a cut groove, consistent with contact between the second stage turbine stator seal plate and the second stage turbine rotor.

The FAA inspector stated that airworthiness directive (AD) 86-08-06 R1 pertained to the accident engine, and required an x-ray inspection of the second stage turbine stator seal plate assembly. The purpose of the AD was to detect and repair engines with second stage turbine stator seal plate assemblies that exhibited warpage. The last annual inspection of the airplane was performed in April 2005, by an airframe and powerplant mechanic with an inspection authorization (IA). According to the aircraft logbooks, the IA noted the AD as "N/A by model #." However, the subject engine model number did require completion of the AD.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# NYC05LA126