N421KC

Destroyed
Minor

Cessna 421CS/N: 421C-0028

Accident Details

Date
Friday, August 5, 2005
NTSB Number
CHI05FA212
Location
Wheeling, IL
Event ID
20050810X01207
Coordinates
42.130001, -87.914443
Aircraft Damage
Destroyed
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The pilot's improper in-flight decision to execute a go-around without raising the landing gear and raising the flaps to the full UP position, resulting in low airspeed and the airplane stalling. Contributing factors to the accident included the pilot's failure to comply with the manufacturer's mandatory service bulletin and the failure of the starter adapter shaft gear which resulted in the loss of power to the left engine, and the collision with the building.

Aircraft Information

Registration
N421KC
Make
CESSNA
Serial Number
421C-0028
Engine Type
Reciprocating
Year Built
1976
Model / ICAO
421CC421
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
SALE REPORTED
Address
545 AVIATION RD
Status
Deregistered
City
OSHKOSH
State / Zip Code
WI 54902-7145
Country
United States

Analysis

HISTORY OF FLIGHT

On August 5, 2005, at 1225 central daylight time, a Cessna 421C, N421KC, was destroyed when it impacted a commercial building and terrain while attempting a go-around about 0.5 miles northwest of the Palwaukee Municipal Airport (PWK), Wheeling, Illinois. The pilot and passenger received minor injuries. The Title 14 Code of Federal Regulations Part 91 personal flight departed from PWK at 1220 and was en route to Mackinac Island, Michigan. Shortly after takeoff, the pilot reported a loss of power to the left engine and circled southeast of the airport to land on runway 34. The pilot attempted to land on runway 34, but executed a go-around. Visual meteorological conditions prevailed at the time of the accident. No flight plan was filed.

The pilot reported that he performed a preflight and departed to the northeast. At 600 feet above ground level (agl) he reduced power to 32.5 inches of manifold pressure (MAP) and 1,900 RPM. The pilot reported that an engine failed. He reported that he identified that the left engine failed and confirmed that the airplane was in a "clean" configuration. He contacted PWK tower and reported that he was returning to PWK for landing.

The pilot reported that he was northeast of PWK when the engine lost power, and that the tower cleared him to land on runway 34. The pilot reported that while he was on the base leg for runway 34, he lowered the flaps to 30 degrees. He reported that he turned on to the final approach course, the airspeed was 115 knots and he planned to "cross the fence" at 100 knots. He lowered the landing gear and lowered the flaps to 45 degrees.

The pilot reported, "Although the descent on final was not too steep, Gear Down, Flaps 45 degrees, and the throttle was in Idle position; I was unable to slow down the aircraft at all. I crossed the fence at 118 KIAS. Because of the excessive airspeed, I overshot the runway. At mid-field, when I realized that a safe landing can not be made, I push the Right throttle full forward and retracted the flaps to 15 degree and then to zero degree. I applied right rudder to maintain directional control and bank 5 degree to the Right. Right after retracting the flaps, I remember moving the landing gear to the UP position. (Although I realized later that the aircraft crashed with the gear in the down position.)"

The pilot reported the when the airplane crossed the fence at the northwest side of the airport, he verified that the mixture, propeller, and throttle were fully forward, and the airplane was in the clean configuration. The pilot reported, "It felt like the RIGHT engine does not produce full power."

The pilot reported that the airspeed continued to decrease and he was not able to gain any altitude. The airplane collided with the roof of a one story industrial building at 15-20 feet, and then impacted a landscape embankment and pine trees. The airplane came to rest on its belly. The pilot reported that he and the passenger evacuated the airplane immediately with only minor injuries.

A witness reported that he observed the airplane attempt to land on runway 34 two times during the same approach. He observed the airplane first attempt to land near the intersection of runway 34 and runway 30, but the airplane ballooned up. The airplane attempted to land again but it ballooned up a second time. The witness heard the pilot add power and attempt a go-around. He reported that the airplane cleared the airport fence, but he lost sight of the airplane behind a tree line. He reported that the landing gear was down during the go-around.

PERSONNEL INFORMATION

The pilot held a private pilot's certificate with single-engine land, multiengine land, and airplane instrument ratings. The pilot reported that he had a total of 728 flight hours with 28 hours in make and model. He held a second-class medical certificate that was issued on September 22, 2004.

The pilot purchased N421KC in May 2005.

AIRCRAFT INFORMATION

The airplane was a twin-engine Cessna 421C, serial number 421C-0028. The airplane seated 8 and had a maximum gross weight of 7,450 pounds. The engines were 375 horsepower Continental GTSIO-520-L engines. The last annual inspection was conducted on March 24, 2005. The airplane had flown about 35 hours since the last inspection and had a total time of about 6,870 hours.

The engine maintenance logbooks indicated that the left and right engines were replaced with overhauled engines on July 17, 1998. As part of the engine overhauls, both engines had the starter adapter shaft gear and crankshaft gear inspection complied with per the Teledyne Continental Motors (TCM) Service Bulletin CSB94-4 along with the installation of the Service Kit EQ6642.

The TCM Service Bulletin CSB94-4 was first issued on June 13, 1994, and the CSB94-4D was reissued as a Mandatory Service Bulletin, MSB94-4E. The latest revision of the Service Bulletin was Mandatory Service Bulletin MSB94-4F, issued on July 5, 2005.

CSB94-4D states the following in GENERAL INFORMATION: "Continued operation of the GTSIO-520 and GIO-550 series engines with starter adapter viscous dampers that have been overheated can lead to distress and possible failure of the starter adapter shaft gear and crankshaft teeth."

A "WARNING" in the Service Bulletin states:

"Compliance with this bulletin is required to prevent possible failure of the starter adapter shaft gear and/or crankshaft gear which can result in metal contamination and/or engine failure."

To comply with the Service Bulletin, the following procedures were required to be followed:

1. Unscheduled maintenance inspection due to rough engine operation (Part 1).

2. At every 100 hour or annual inspection (which ever occurs first) perform the inspections detailed in Part 2, "STARTER ADAPTER VISCOUS DAMPER and SHAFTGEAR BACKLASH INSPECTION".

3. Starter adapters with less than 400 hours total time in service must be inspected in accordance with the "VISUAL INSPECTION PROCEDURE" set forth in Part 3 of this bulletin upon the accumulation of 400 hours total time in service and every 400 hours time in service thereafter.

4. Starter adapters with more than 400 hours total time in service must be inspected in accordance with the "VISUAL INSPECTION PROCEDURES" set forth in Part 3 of this bulletin within the next 25 hours of operation and every 400 hours thereafter.

5. If needle bearing P/N 537721 is installed in the crankcase, it must be removed and replaced with the bushing P/N 654472. Refer to Part 3, paragraph 9 and also Part 4 on page 10 for installation instruction. Order bushing P/N 654472 separately, if required.

6. If service kit P/N EQ 6642R has not been installed prior to engine overhaul it must be installed at the next engine overhaul or at the time of starter adapter replacement, whichever occurs first. Refer to the latest revision of TCM SB97-6 or mandatory replacement parts. Refer to Part 5 for instructions for installing service kit EQ 6642R.

NOTE: Both the crankshaft gear and the starter adapter assembly, included in EQ 6642R, must be replaced at the same time if the tooth wear of either the crankshaft gear or the starter adapter shaft gear is unacceptable in accordance with this bulletin.

The left and right engine logbooks indicated that neither the TCM Service Bulletin CSB94-4 nor Mandatory Service Bulletin CSB94-4E had been complied with since the engines had been overhauled on July 17, 1998. The engines had accumulated about 1,272 hours since the last overhaul.

The Federal Aviation Administration (FAA) issued Airworthiness Directive (AD) 2005-20-04 on November 1, 2005. The AD stated, "We are issuing this AD to prevent failure of the starter adapter assembly and or crankshaft gear, resulting in failure of the engine and possible forced landing." The AD further stated, "You must use TCM Mandatory Service Bulletin No. MSB94-4F, dated July 5, 2005, to perform the actions required by this AD."

METEOROLOGICAL INFORMATION

The observed weather at PWK at 1253 was: Winds 070 degrees at 9 knots, sky clear, visibility 10 statute miles, temperature 26 degrees Celsius, dew point 16 degrees Celsius, altimeter 30.24 inches of mercury.

WRECKAGE AND IMPACT INFORMATION

The airplane impacted a one-story industrial building, and then impacted a landscape embankment and pine trees. The wreckage path was about 114 feet in length on a westerly heading. The location of the main wreckage was coordinates 42 degrees 7 minutes 42 seconds north latitude, 087 degrees 54 minutes 52 seconds west longitude. The airplane remained upright and there was no ground fire. The main landing gear and nose landing gear were found separated from the fuselage. The left wing was partially separated from the fuselage near the wing root. The left and right wing fuel tanks were full of fuel. The landing gear handle was in the down position. The flap lever and indicator were about 1/4 down. The split flaps were found extended about 15 degrees. The left propeller was found in the feathered position. The right propeller blades exhibited leading edge gouges and chordwise scratching.

The on-site inspection of the right engine revealed that the crankshaft rotated and drive train continuity was confirmed. All cylinders exhibited thumb compression.

The on-site inspection of the left engine revealed that the idler gear support pin had separated from the engine and was found lying in the engine accessory section. The two studs that held the idler gear support pin to the crankcase were sheared off.

The left and right engines were shipped to the engine manufacturer for teardown inspections.

TESTS AND RESEARCH INFORMATION

The left and right engines were sent to Teledyne Continental Motors (TCM) for engine teardowns on October 4, 2005, with the National Transportation Safety Board investigator-in-charge (IIC) providing oversight.

The inspection of the left ...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI05FA212