N7546T

Substantial
None

American Champion (ACAC) 7KCABS/N: 287-70

Accident Details

Date
Monday, August 22, 2005
NTSB Number
SEA05LA179
Location
Richland, WA
Event ID
20050831X01349
Coordinates
46.367221, -119.306388
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The oil pressure gauge line fitting coming loose from the engine, resulting in the loss of oil to the point where internal engine components were starved for oil, leading to extensive internal damage and seizing of the engine. Factors include a set of eight inch high berms in the field where the pilot found it necessary to execute his forced landing.

Aircraft Information

Registration
N7546T
Make
AMERICAN CHAMPION (ACAC)
Serial Number
287-70
Engine Type
Reciprocating
Year Built
1960
Model / ICAO
7KCABCH7B
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
CARGILE WILLIAM T
Address
CARGILE JESSIE M
13 B ST
Status
Deregistered
City
ROSWELL
State / Zip Code
NM 88201
Country
United States

Analysis

On August 22, 2005, approximately 0835 Pacific daylight time, an American Champion 7KCAB, N7546T, nosed over during a forced landing in an open field about three miles north of Richland, Washington. The private pilot, who was the sole occupant, was not injured, but the aircraft, which is owned and operated by the pilot, sustained substantial damage. The local 14 CFR Part 91 personal pleasure flight, which departed Richland about 35 minutes prior to the accident, was being operated in visual meteorological conditions. No flight plan had been filed. The ELT, which was activated by the accident sequence, was turned off at the scene.

According to the pilot, he had just finished practicing a series of aerobatic maneuvers, and was descending back toward the airport when the engine suddenly quit. He attempted to restart the engine, which momentarily fired, but it did not stay running. The propeller, which initially was windmilling after the power loss, eventually came to a stop, and the pilot was unable to get the engine to rotate by activating the starter. He therefore made a power-off forced landing in a nearby open field. Although the flare and touchdown were uneventful, during the landing roll, the aircraft encountered a pair of eight inch high berms, that appeared to have been created by a bulldozer, and subsequently nosed over onto its back.

A post-accident inspection of the aircraft and engine determined that the fitting that attaches the oil pressure gauge line to the engine had come loose, and oil had escaped from the area around the fitting. Further inspection revealed that the loss of oil lead to extensive thermal and mechanical damage to the primary lower end engine components, and that the engine had seized as a result of that damage. A review of the aircraft records did not reveal any recent maintenance in which the oil pressure measuring system would have been expected to have been manipulated.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA05LA179