N928MB

Substantial
None

Mooney M20KS/N: 25-0859

Accident Details

Date
Sunday, May 29, 2005
NTSB Number
DEN05LA139
Location
Englewood, CO
Event ID
20050926X01531
Coordinates
39.569999, -104.849166
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

the pilot's failure to maintain control of the airplane and the pilot's improper use of unusual attitude recovery procedure. Contributing factors were the failure of the HSI and the clouds.

Aircraft Information

Registration
Make
MOONEY
Serial Number
25-0859
Engine Type
Reciprocating
Year Built
1985
Model / ICAO
M20KM20T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
M20K

Registered Owner (Current)

Name
TRAVELING PALS III LLC
Address
3340 ROYALSTON AVE
City
FORT MYERS
State / Zip Code
FL 33916-1623
Country
United States

Analysis

On May 29, 2005, approximately 0930 mountain daylight time, a Mooney M20K, N928MB, piloted by a private pilot, was substantially damaged when it was overstressed after departing Centennial Airport (APA), Englewood, Colorado. Instrument meteorological conditions prevailed at the time of the accident. The personal cross-country flight was being conducted under the provisions of Title 14 CFR Part 91. An instrument flight rules flight plan had been filed. The pilot, the sole occupant of the airplane, sustained no injuries. The flight originated at APA approximately 0900 and was en route to Camarillo Airport (CMA), Camarillo, California.

According to the pilot, he was in instrument meteorological conditions and climbing to his cruise altitude when the horizontal situation indicator (HSI) failed. He became disoriented, the airplane got into an unusual attitude, and he lost control of the airplane. When the airplane broke out of the clouds, it was descending rapidly, and he pulled back hard on the control yoke to arrest the descent. During the recovery, the airplane's structural limitations were exceeded and the airplane was overstressed.

According to a telephone interview with a mechanic who replaced the HSI at Duncan Aviation, a repair shop located at APA, a plastic gear in the HSI was "stripped" and the heading bug caused the compass card to "hang-up."

According to an FAA airworthiness safety inspector, the wing was wrinkled and the accompanying rivets were "popped." Damage to the wing was such that the insurance company wrote off the airplane as a total loss. The pilot was unaware of the damage to the airplane and had flown it on numerous occasions after the accident. When the damage was brought to his attention, he reported the accident.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# DEN05LA139