N7684G

Substantial
None

Cessna 172LS/N: 17259384

Accident Details

Date
Tuesday, November 8, 2005
NTSB Number
NYC06LA028
Location
Lehighton, PA
Event ID
20051118X01857
Coordinates
40.844165, -75.635559
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot's inadequate preflight inspection, which resulted in a total loss of engine power during takeoff due to fuel contamination, and a subsequent forced landing to a field.

Aircraft Information

Registration
N7684G
Make
CESSNA
Serial Number
17259384
Engine Type
Reciprocating
Year Built
1970
Model / ICAO
172LC172
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SELLIX DOUGLAS W
Address
100 COURT STREET
Status
Deregistered
City
LEHIGHTON
State / Zip Code
PA 18235
Country
United States

Analysis

On November 8, 2005, about 1415 eastern standard time, a Cessna 172L, N7684G, was substantially damaged during a forced landing, following a total loss of engine power while departing Beltzville Airport (14N), Lehighton, Pennsylvania. The certificated airline transport pilot was not injured. Visual meteorological conditions prevailed for the planned flight to Slatington Airport (69N), Slatington, Pennsylvania. No flight plan was filed for the personal flight conducted under 14 CFR Part 91.

During an interview with a Federal Aviation Administration (FAA) inspector, the pilot reported that the airplane had not flown for several weeks.

According to the pilot's written statement, he intended to fly the airplane to a nearby airport and have an annual inspection performed. The pilot further stated that he sumped both fuel tanks and the gascolator during the preflight inspection. In addition, the taxi and engine run-up were normal. The airplane subsequently departed on runway 26, a 2,020-foot-long, 100-foot-wide, turf runway. About 250 feet above the ground, the engine began to run rough and lose power. The pilot turned right to avoid obstacles, and the engine lost all power. The pilot then attempted a forced landing to a field, but the airspeed decreased, and the rate of descent increased. The airplane's nosegear impacted a down-sloping field. During the impact, the left wing sustained substantial damage from a tree strike, and the airplane came to rest upright in the field.

The FAA inspector recovered approximately 4 ounces of fluid from the carburetor. About 3 1/2 ounces were consistent with water, while 1/2 ounce was consistent with fuel.

The pilot stated that he was unable to locate the aircraft logbooks. In addition, after one verbal and two written requests from a Safety Board investigator, the pilot failed to provide information regarding the date of the airplane's last annual inspection, or the airframe total time at that inspection.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# NYC06LA028