N469MD

Destroyed
Fatal

Beech 58PS/N: TJ-331

Accident Details

Date
Thursday, February 23, 2006
NTSB Number
SEA06FA054
Location
Bow, WA
Event ID
20060301X00257
Coordinates
48.542778, -122.404724
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
1
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The pilot's failure to maintain aircraft control during the climb to cruise. Contributing factors included a loss of engine power to the right engine folowing a turbocharger failure, instrument meteorological and dark night conditions.

Aircraft Information

Registration
N469MD
Make
BEECH
Serial Number
TJ-331
Engine Type
Reciprocating
Year Built
1981
Model / ICAO
58PB58T
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
H & W MANAGEMENT SERVICES INC
Address
447 LAGUNA RD
Status
Deregistered
City
PASADENA
State / Zip Code
CA 91105-2218
Country
United States

Analysis

HISTORY OF FLIGHT

On February 22, 2006, about 1854 Pacific standard time, a Beech 58P Baron, N469MD, was destroyed when it collided with terrain subsequent to a reported loss of engine power during the initial climb out approximately two nautical miles south of Bow, Washington. The airplane was registered to H&W Management Services, Inc, of Carson City, Nevada, and was being operated by the pilot as an instrument flight rules (IFR) cross-country flight under the provisions of Title 14, CFR Part 91, when the accident occurred. The commercial pilot, the sole occupant of the airplane, was fatally injured. Night instrument meteorological conditions prevailed at the time of the accident, and an instrument flight rules (IFR) flight plan was in effect. The flight originated from the Bellingham Regional Airport about 1843 Pacific standard time, and was en route to the Ogden International Airport, Ogden, Utah.

Recorded air traffic control (ATC) communications between Seattle Air Route Traffic Control Center, and the pilot of N469MD, indicated the pilot radioed Seattle Center communicating that he was out of 7,800 feet. Seattle Center acknowledged the pilot and cleared the airplane to 15,000 feet. Shortly thereafter, Seattle Center received a "mayday" transmission followed by "lost an engine." Shortly after the transmission, radio and radar contact with the airplane were lost.

Witnesses reported they observed the airplane in an unusually steep descent prior to impacting terrain. One witness stated he heard a high-pitched noise emanating from the airplane as it descended toward the ground.

The wreckage was located in an open field adjacent to Highway 11. The main wreckage was located in the confines of a large impact crater approximately 15 feet in diameter and 6 feet deep.

PERSONNEL INFORMATION

The pilot held a private pilot certificate with an airplane single-engine land rating, a commercial certificate with a multi-engine land rating and a commercial instrument airplane rating. The pilot's most recent medical certificate (third-class) was issued on June 26, 2004. The certificate carried a limitation requiring the pilot to wear corrective lenses.

Comprehensive flight time logbooks for the pilot were not located. Documentation was located indicating the pilot completed a flight review (FAR 61.56) and an instrument proficiency check (FAR 61.57[d]) on October 22, 2005.

On the pilot's latest FAA Application for Airman Medical Certificate (Form 8500-8), dated June 26, 2004, the pilot listed 7,500 hours total pilot time and 150 hours total pilot time in the 6 months preceding the medical.

AIRCRAFT INFORMATION

The twin engine Beech Baron 58P, serial number TJ-331, was manufactured in 1978 and was certified as a normal category airplane. The airplane was equipped with two Teledyne Continental Motors (TCM) TSIO-520 engines, each rated at 310 horsepower. The airplane was approved for visual flight rules (VFR) and instrument flight rules (IFR) operations, as well as flight in icing conditions.

The airplane's last inspection, an annual inspection, was completed on December 16, 2005. Maintenance records showed the airplane's total time at inspection was 9,401 hours. The right engine's total time at inspection was 2,048 hours (621 since major overhaul); the left engine's total time at inspection was 3,476 hours (695 since major overhaul). A top overhaul of both engines was completed during the annual inspection.

Maintenance records showed that the last altimeter system and altitude reporting equipment test (in accordance with FAR 91.411) was completed on June 24, 2004.

Complete airframe, engine and propeller maintenance logbook records were not located for the accident aircraft.

METEOROLOGICAL INFORMATION

The closest weather observation facility to the accident site was the Skagit Regional Airport (KBVS), located approximately 4.6 miles south of the accident location at an elevation of 144 feet msl. The airport is equipped with an Automated Weather Observation System (AWOS). The following Meteorological Aerodrome Reports (METARs) were issued surrounding the period of the accident:

On February 22, at 1850, the METAR observation was, in part, winds from 180 degrees at 4 knots, visibility 8 statute miles, a few clouds at 2,000 feet, overcast skies at 3,500 feet, temperature 4 degrees C.

At 1910, the METAR observation was, in part, visibility 7 statute miles, scattered clouds at 100 feet, broken clouds at 2,500 feet, overcast skies at 3,400 feet, temperature 4 degrees C.

COMMUNICATIONS

At 1851:02, the pilot of N469MD was instructed by Whidbey Approach to contact Seattle Center on frequency 134.95. The pilot acknowledged the ATC specialist and subsequently contacted Seattle Center stating he was through 7,800 for niner (nine) thousand. The ATC specialist then cleared the aircraft to 15,000 feet, and at 1851:38 the pilot acknowledged the clearance, stating, "we're up to one five thousand for niner mike delta."

At 1853:43, ATC received an unintelligible radio transmission containing "lost a" and "niner mike delta."

At 1853:48, ATC received a second transmission from the pilot who stated "mayday mayday just lost an engine a."

At 1853:53 and 1853:55, ATC received two additional transmissions believed to be from the pilot, however both were unintelligible.

This was the last known radio transmission from the pilot of the accident aircraft.

A complete ATC communication transcript and radar data are included in the public docket.

FLIGHT RECORDERS

The airplane was not equipped with flight data or cockpit voice recorders.

WRECKAGE AND IMPACT INFORMATION

Personnel from the National Transportation Safety Board, Federal Aviation Administration, Teledyne Continental Motors and Raytheon Aircraft accessed the aircraft wreckage on February 23-24, 2006.

The crash site was located in an open field adjacent to the intersection of Highway 11 and Sunset Road, at 48 degrees 32.56 minutes' north latitude and 122 degrees 24.28 minutes' west longitude. The elevation at the crash site was approximately 11 feet above mean sea level (msl). The surrounding terrain was relatively flat and featureless.

The wreckage debris field encompassed an area approximately 348 feet in length (from south to north). The main wreckage was located in the confines of a large impact crater measuring approximately 15 feet in diameter and 6 feet deep. A majority of the wreckage was located in the immediate area of the impact crater. Numerous small pieces of system components and cockpit instrumentation were scattered from the crater to the end of the wreckage debris path.

The main wreckage included engines and propeller assemblies, fuselage, wing assemblies, and tail assembly. Impact forces destroyed the forward section of the fuselage and cockpit. A majority of the cockpit components and instrumentation were located in the crater and were severely fragmented. Both engine assemblies were separated from the airframe and located near the bottom of the crater. Both assemblies sustained extensive impact related damage. The 3-bladed McCauley propeller assemblies were located within the confines of the crater. Both sustained extensive impact related damage. The six propeller blades were separated from their respective hub assemblies and were located in the confines of the impact crater. Forward bending, leading edge damage, chord wise scratches and extensive overall deformation were noted to the propeller blades. The main wing assembly was located with the main wreckage and sustained extensive impact related damage and fragmentation. Extensive accordion type damage was noted to the leading edge of the wing structure. The entire wing assembly was severely fragmented and deformed. Both flap and aileron assemblies were attached to the wing structure and sustained impact related damage. The aileron trim actuator measured 1.5 inches, which equates to 4.75 degrees tab up. Flap actuator measurements indicated the flaps were in the up position at the time of impact. The remains of the empennage assembly were located near the center of the impact crater, atop of the main wreckage. The vertical stabilizer was bent forward and the rudder was separated from the assembly. The horizontal stabilizers remained attached to the empennage assembly, but sustained extensive impact related damage. The right-hand and left-hand elevators were attached to the empennage and extensive bending deformation was noted. The elevator trim tab actuators measured 1.08 inches, which corresponds to 5 degrees tab down. The rudder trim actuator measured 4 inches, which equates to approximately 4 degrees tab left. The landing gear was located in the confines of the impact crater. It was determined that the landing gear was in the up position prior to impact.

All primary flight control surfaces and major system components were identified and located at the wreckage site prior to the wreckage being recovered.

The impact crater was full of water and oil. There was a strong odor of aviation fuel in and around the accident site.

Reexamination of the wreckage on October 3, 2006, by investigators from National Transportation Safety Board and Raytheon Aircraft, focused on the right engine's induction system. The induction system sustained impact related damage and was heavily distorted, however, the alternate air door and hinge assembly were intact.

MEDICAL AND PATHOLOGICAL INFORMATION

Representatives from the Skagit County Coroner's Office, Mount Vernon, Washington, performed the autopsy on the pilot on February 23, 2006. According to the autopsy report, the pilot's cause of death was determined to be "blunt trauma to head, trunk & extremities."

Toxicological testing of specimens from the pilot was performed by the FAA Forensic Toxicology Research Team, Oklahoma City, Oklahoma. The report stat...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA06FA054