N688JK

Substantial
None

Robinson R44S/N: 45012

Accident Details

Date
Tuesday, May 30, 2006
NTSB Number
ANC06LA064
Location
Skwentna, AK
Event ID
20060531X00646
Coordinates
62.122222, -151.235549
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The pilot's improper rigging of the external sling load, which allowed the suspended load/cargo cable to entangle and disable the tail rotor control, resulting in a loss of control during cruise and an in-flight collision with terrain.

Aircraft Information

Registration
N688JK
Make
ROBINSON
Serial Number
45012
Engine Type
Reciprocating
Year Built
2003
Model / ICAO
R44R44
Aircraft Type
Rotorcraft
No. of Engines
1

Registered Owner (Historical)

Name
ACE FLYERS INC
Address
1842 MERRILL FIELD DR
Status
Deregistered
City
ANCHORAGE
State / Zip Code
AK 99501-4112
Country
United States

Analysis

On May 29, 2006, about 1920 Alaska daylight time, a skid-equipped Robinson R44 helicopter, N688JK, operated by Ace Flyers, dba JayHawk Air, Anchorage, Alaska, had a loss of tail rotor effectiveness during an emergency landing, and sustained substantial damage when it collided with terrain, about 17 miles north-northwest of Skwentna, Alaska. The commercial certificated pilot and the sole passenger reported no injuries. The local flight was operating in day visual meteorological conditions as an on-demand, Title 14, CFR Part 135 air taxi flight when the accident occurred.

During a telephone conversation with the NTSB investigator-in-charge (IIC) on May 30, the pilot reported that he was repositioning the passenger and a wire mesh cage from a remote drilling site near Sable Creek to a site nearby on the Kahiltna River. The pilot related that the wire cage was slung underneath the helicopter on a line about 18 feet long. He stated that about a minute after liftoff from the 1,200 feet msl site, following the transition to cruise flight, he looked outside the helicopter to try and see how the load was positioned. He said he could not visually acquire the load, and he suddenly heard an unusual noise and felt a shudder/vibration. He immediately jettisoned the load, and sought an emergency landing site close by. The landing site was a clear area in alder brush, on about a 15 degree slope. The pilot reported that the helicopter continued to vibrate and make unusual sounds as he came to a 2 foot hover over the landing site. When he increased the main rotor pitch with the collective control, the pilot said he stepped on the tail rotor control pedals, but there was "no pedal" and no response from the tail rotor. The helicopter quickly started to rotate, and immediately rolled onto its side as it touched the ground. The pilot stated that it was likely that the load on the tether line somehow struck or interfered with the tail rotor, although he could not see any damage to the tail rotor after landing.

In his written statement to the NTSB, the pilot wrote in the section titled: Recommendation (How Could This Accident Have Been Prevented), "Pilot Error--I allowed a light load to catch the tip of the tail rotors."

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ANC06LA064