N117PS

Substantial
None

Aviat Aircraft Inc Pitts S-2BS/N: 5346

Accident Details

Date
Saturday, June 3, 2006
NTSB Number
LAX06LA190
Location
Antioch, CA
Event ID
20060607X00712
Coordinates
37.933334, -121.783332
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The loss of oil pressure due to metal pieces from the number 5 piston skirt in the oil system, which prevented the oil valve top ball valve from seating. The muddy terrain was a factor.

Aircraft Information

Registration
N117PS
Make
AVIAT AIRCRAFT INC
Serial Number
5346
Engine Type
Reciprocating
Year Built
1996
Model / ICAO
Pitts S-2BAT2P
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
TEAM FOUMORI LLC
Address
2040 LAGUNA ST APT 302
Status
Deregistered
City
SAN FRANCISCO
State / Zip Code
CA 94115-2371
Country
United States

Analysis

On June 3, 2006, at 1435 Pacific daylight time, an Aviat Aircraft Incorporated Pitts S-2B, N117PS, lost oil pressure in flight and the pilot performed a precautionary landing to a hay field in Antioch, California. The airplane nosed over and sustained substantial damage. The commercial pilot, the sole occupant, was not injured. The airplane was registered to a private company and the pilot was operating it under the provisions of 14 CFR Part 91. Visual meteorological conditions prevailed and no flight plan had been filed for the local, personal aerobatic flight. The pilot departed from Livermore Municipal Airport, Livermore, California, at 1400.

The pilot reported that while performing an aerobatic sequence, the engine lost oil pressure and he elected to perform a precautionary landing in a field. The pilot shutdown the engine after 15 seconds when he had his landing spot secured. During the landing roll, the airplane nosed over in the muddy terrain.

The Federal Aviation Administration accident coordinator examined the engine following the accident. The engine oil sump contained approximately 9 quarts of oil. The oil pressure gauge was tested and no operational anomalies were noted. The engine was test-run; however, the oil pressure gauge did not indicate positive pressure. The oil pump was removed from the accessory case and was turned by hand. Oil was present within the oil pump and coated the gears and shaft. No heat signatures were evident.

The airplane was equipped with a Christen inverted oil system. The oil valve works through the means of gravity operated ball valves which includes two balls and a spring. During normal flight, the top ball valve is closed and the bottom ball valve is open. During inverted flight, the opposite is true. The oil valve was disassembled. Within the valve, a metal piece approximately 0.5-inch in length was identified between the two balls.

Later disassembly of the engine showed that portions of the number 5 piston skirt had fractured from the piston. Pieces of the fractured skirt were identified in the oil sump and filter.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX06LA190