N486SB

Destroyed
Fatal

Cessna 560S/N: 560-0580

Accident Details

Date
Sunday, June 25, 2006
NTSB Number
LAX06FA211
Location
Upland, CA
Event ID
20060629X00851
Coordinates
34.109165, -117.695831
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
1
Serious Injuries
2
Minor Injuries
0
Uninjured
0
Total Aboard
3

Probable Cause and Findings

The pilot's unstabilized approach to the runway and failure to obtain the proper touchdown point, which resulted in a runway overrun.

Aircraft Information

Registration
N486SB
Make
CESSNA
Serial Number
560-0580
Engine Type
Turbo-jet
Year Built
2001
Model / ICAO
560C560
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
AERO CHARTER SERVICES INC
Address
3411 SILVERSIDE RD
103 SPRINGER BLDG
Status
Deregistered
City
WILMINGTON
State / Zip Code
DE 19810
Country
United States

Analysis

1.1 History of the Flight

On June 24, 2006, at 2226 Pacific daylight time, a Cessna 560, N486SB, collided with obstacles and terrain following a runway overrun at Cable Airport, Upland, California. The airplane was registered to Aero Charter Services, Incorporated and the commercial pilot (the president of Aero Charter Services, Incorporated) was operating the airplane under the provisions of 14 CFR Part 91 using a single-pilot waiver. The pilot and two passengers sustained serious injuries; the airplane was destroyed. Night visual meteorological conditions prevailed and the pilot canceled his instrument flight rules clearance at 2221 when he reported obtaining visual contact with Cable Airport. The pilot departed from Montgomery Field, San Diego, California, at 2200, and was landing at his destination when the accident occurred. One of the passengers later succumbed to her injuries.

According to friends of the pilot, the pilot, his wife, and his daughter, were attending a personal event in San Diego. They were returning to their home-based airport when the accident occurred. The pilot had been based at the airport for about 2 years.

1.1.1 Witness Information

A witness, who was a pilot and airplane builder, was standing at the Experimental Aircraft Association (EAA) chapter hangar located on the northeast side of the airport, when the airplane landed on runway 24. He noted a 5 to 7 knot tailwind from the east. When the accident airplane touched down, the airplane was approximately 1,000 to 1,300 feet down the 3,864-foot runway. He heard the engines spool up and then it was quiet. The landing approach was not consistent with landings that the witness had previously seen the pilot of N486SB conduct. Normally when the pilot would land the airplane, he would touch down directly onto the numbers of the runway.

Additional witnesses were sitting in their home, which was located in a rock quarry plant at the end of runway 24. They heard the airplane and looked out the window. As it passed by four big hangar doors, they could hear the thrust reversers and the airplane kept rolling off the end of the runway. The witness stated, "It appeared like the pilot wanted to climb the airplane." They then witnessed flames shooting up from the accident area. The witnesses noted that it appeared the airplane did not have the runway distance it needed to land.

Another witness, reported that he did not see the airplane coming into land. He could hear the airplane and it sounded as if it were taking off. He then heard the sound of "reverse thrust" prior to the airplane powering up again. As the airplane came into view from behind a building, it was low to the ground and climbing. When it was about 20 to 40 yards above ground level, the witness heard the thrust reversers again and the airplane nosed down into the ground where it impacted an embankment and exploded into flames.

An additional witness, who was a police officer, reported that he did not see the airplane but heard it fly over his house. He had heard the airplane fly over many times in the past and was familiar with his approach. As the airplane came over his house, it sounded lower than normal like the engines were spooled down. Normally, about 20 to 25 seconds later he hears the sound of the thrust reversers but he did not hear them deploy.

1.2 Performance Information

The airplane was equipped with a Honeywell enhanced ground proximity warning system (EGPWS) unit. The unit does not record event times or dates, but tracks the duration of an event and each leg. The flight history was downloaded from the EGPWS unit at Honeywell, Redmond, Washington, on July 31, 2006, with the National Transportation Safety Board (NTSB) investigator and representatives from Honeywell present. The accident flight was identified as the last recorded event in the unit.

1.2.1 Performance Study

An NTSB performance engineer completed a performance study using data obtained from the Honeywell EGPWS, the Cockpit Voice Recorder (CVR), reported atmospheric data, and airplane data from Cessna's airplane flight manual. The results of the study indicated that the airplane approached runway 24 for landing, above the 4-degree visual glide slope indicator. During the approach, the data showed two periods of sink rate warnings, and then about 11 seconds after the last warning the data indicated that the airplane touched down about 1,400 feet beyond the runway 24 displaced threshold. The published total landing length of runway 24 is 3,707 feet. Landing distance calculations revealed that the distance required for a full stop landing after touchdown was between 3,072 and 4,524 feet for the given conditions. According to the engineer, the accident flight needed an additional 765 to 2,217 feet of runway for a full stop landing.

During the approach, two sink rate warnings were issued; one was issued about 1,500 feet horizontally from the threshold and the other was issued about 700 feet horizontally from the threshold. The engineer further reported that the sound of touchdown occurred about 11 seconds after the last sink rate warning, placing the airplane at a minimum, about 1,400 feet past the runway 24 displaced threshold.

1.3 Cockpit Voice Recorder Information

A Fairchild Model A200S 2-hour solid-state CVR (serial number unidentifiable) was delivered to the audio laboratory of the National Transportation Safety Board on June 27, 2006. The event was captured near the end of the recording. A CVR Group was not convened.

The CVR engineer indicated that at 2221:35, the pilot radioed that he was on the vhf-omnidirectional range (VOR) approach into Cable and would be entering the downwind for runway 24. He canceled his instrument clearance and at 2223:03, the pilot radioed that he was established on the downwind leg for Cable Airport. At 2224:26 the pilot indicated that he was turning base. At 2224:50, there was a sound consistent with six radio on-off key clicks being performed in rapid succession. At 2224:56, the pilot called again stating that he was turning base. A series of messages related to minimums and sink rate were heard and at 2225:51, the sound of touchdown was heard. The recording ended at 2226:10.

1.4 Pilot Information

The pilot held a commercial pilot certificate with ratings to fly single- and multi-engine airplanes under instrument conditions. The pilot held a second-class medical certificate that was issued on September 9, 2005. It contained the restriction that the pilot must wear lenses for distant and possess glasses for near vision. On the application, the pilot reported a total flight time of 2,700 hours.

The pilot attended training at CAE Simuflight, in Fort Worth, Texas. On April 18, 2006, the pilot obtained a single pilot certification by Federal Aviation Administration exemption to operate the Cessna Citation CE-560-Ultra, CE-560-Encore aircraft. The certification was valid through April of 2007.

The pilot's attorney submitted the completed National Transportation Safety Board (NTSB) form 6120.1/2, the Pilot Operator Report, on behalf of the pilot. On the form a total flight time of 2,951 flight hours was reported, with 268 hours in the accident make/model airplane. A total of 50 hours of night flight time was recorded. No flight times were reported for the past 90 and 30 days. The pilot indicated on the form that he could not recall the circumstances that led to the accident.

1.5 Airplane Information

The airplane was a Cessna 560 Citation manufactured in 2001 and was certified by the FAA requiring a two-person flight crew. It was equipped with two model PW535A Pratt and Whitney Canada engines. Federal Aviation Administration records show that the airplane was purchased by Aero Charter Services, Incorporated on August 5, 2005.

On June 24, the airplane was fueled with 500 gallons of Jet A at Crown Air, located at Montgomery Field.

The airplane was maintained through a phase inspection program. The last completed inspections were Phase 8, Phase 11, Phase 23, and Phase 54 inspections. They were completed on May 7, 2006, at an airframe time of 2,513 hours. The engines had also accrued 2,513 hours at the time of the phase inspections. About 30 hours had accumulated on the airplane since the last inspections.

1.6 Airport Information

The Airport Facility Directory/Southwest shows that Cable Airport runway 06/24 is 3,864 feet in length and 75 feet wide. The runway is equipped with medium intensity runway edge lights. Both runways are served by 2-box visual approach slope indicators with 4-degree glide paths. There are no runway end identifier lights. The airport has two instrument approach procedures that include a global positioning system (GPS) for runway 06 and a VOR for runway 06.

1.7 Meteorological Information

Recorded winds were obtained from a local fixed base operator at the Cable airport. At 2216, winds were 3.5 knots from the south-southeast. At 2231, winds were 3.5 knots from the south-southeast. At 2246, winds were 4.3 knots from the southeast.

The winds reported at the Ontario International Airport, Ontario, California, at 2153, located 6 nautical miles southeast of the accident site were calm.

1.8 Wreckage and Impact Information

The NTSB investigator, an inspector from the FAA Riverside Flight Standards District Office, a representative from Cessna Aircraft Company, a party to the investigation, and an advisor from Pratt and Whitney Canada, responded to the accident site on June 25, 2006. The airplane came to rest approximately 851 feet beyond the departure end of runway 24, and was extensively burned. The general wreckage path was in the direction of 240 degrees.

An examination of the runway surface did not reveal the presence of any skid marks or rubber debris consistent with the tires on the airplane. From the end of the runway, a dirt overrun area extended before the terrain ...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX06FA211