N4233J

Substantial
Serious

Storm Zenair CH-701S/N: 3957028

Accident Details

Date
Sunday, July 9, 2006
NTSB Number
ANC06LA086
Location
Fairbanks, AK
Event ID
20060720X00973
Coordinates
64.853614, -147.402221
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The total loss of engine power for an undetermined reason during cruise flight, which resulted in an emergency descent into trees.

Aircraft Information

Registration
Make
STORM
Serial Number
3957028
Engine Type
Reciprocating
Year Built
1991
Model / ICAO
Zenair CH-701
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
ZENAIR CH-701

Registered Owner (Current)

Name
PEET TIMOTHY C
Address
PO BOX 75
City
KREMLIN
State / Zip Code
MT 59532-0075
Country
United States

Analysis

On July 9, 2006, about 1455 Alaska daylight time, a Storm Zenair CH-701 experimental amateur-built airplane, N4233J, sustained substantial damage when it collided with brush covered terrain during an emergency landing following a loss of engine power, about 9 miles east of Fairbanks, Alaska. The airplane was operated by the pilot as a visual flight rules (VFR) personal cross-country flight under Title 14, CFR Part 91, when the accident occurred. The solo sport pilot certificated pilot received serious injuries. Visual meteorological conditions prevailed, and no flight plan was filed. The flight originated at the Chena Marina Airport, Fairbanks, about 1345, and was bound for Bradley Airfield, North Pole, Alaska.

During a telephone conversation with the National Transportation Safety Board (NTSB) investigator-in-charge (IIC) on July 18, the pilot said he had been in the air for about 30 minutes en route to his destination when the airplane's engine "stuttered and then quit." He said during the emergency landing the airplane impacted brush covered terrain. The pilot said the airplane sustained structural damage to the left wing, fuselage, and horizontal stabilizer. He indicated there were no known mechanical anomalies with the airplane prior to the accident. He reported that the engine had quit previously due to a failed seal, but the airplane's engine had been rebuilt, and he had flown 45-50 hours since the rebuild. The pilot was unaware of what precipitated the loss of engine power on the accident flight. The airplane was not examined by an NTSB investigator.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ANC06LA086