Accident Details
Probable Cause and Findings
The failure of the glider pilot to utilize his transponder and the high closure rate of the two aircraft, which limited each pilot's opportunity to see and avoid the other aircraft.
Aircraft Information
Registered Owner (Current)
Analysis
"THIS CASE WAS MODIFIED ON MARCH 5, 2008."
1.1 HISTORY OF FLIGHT
On August 28, 2006, at 1506 Pacific daylight time, a Raytheon Aircraft Company Hawker 800XP transport airplane, N879QS, and a Schleicher ASW27-18 glider, N7729, collided in midair about 10 miles west-northwest of Smith, Nevada. Both airplanes sustained substantial damage. The Hawker flight crew (both airline transport pilots) sustained minor injuries, while their three passengers were not injured. The glider pilot (a private pilot) received minor injuries. The Hawker 800XP was fractionally owned by different corporations and managed by NetJets Aviation, Inc., of Columbus, Ohio. Its flight was being conducted under the provisions of 14 CFR Part 91 Subpart K as an executive/corporate flight. The glider was registered to a private individual and was operated by the pilot under the provisions of 14 CFR Part 91 as a personal flight. An instrument flight rules flight plan was filed for the Hawker, which began its flight from Carlsbad, California, at 1400, and was destined for Reno, Nevada. No flight plan had been filed for the glider, which was on a local flight that had departed Minden, Nevada, at 1300. Visual meteorological conditions prevailed at the time of the collision.
1.1.1 Hawker 800XP Flight Crew Statements
According to interviews conducted by the NTSB investigator-in-charge (IIC), the flight crew indicated that they were cleared by air traffic control from 16,000 feet to 11,000 feet. The captain was the flying pilot and the first officer was working the radios. Oakland Air Route Traffic Control Center (ARTCC) transferred the flight to Reno approach control just prior to the collision. The first officer tuned in the Reno approach control radio frequency and looked out the right cockpit window. He then heard the captain shout and the audio tone for the autopilot, and noted that the captain had pushed the control yoke down and to the right. As he was turning his head to see what was going on, he observed the captain's side of the instrument panel "explode."
The captain reported that they were cleared to descend and as she looked outside she noted something out of the corner of her eye to the left. As she looked to the left, she noted a glider filling the windshield. She moved the control yoke down and to the right in an attempt to avoid hitting the glider.
The first officer and captain reported that the cockpit was noisy with wind after the collision, and the captain's headset had been knocked off. The first officer attempted to communicate with Reno controllers but had difficulty. The captain recovered the airplane as the first officer communicated to Reno that they had some sort of structural problem (he later learned that they had collided with a glider) and declared an emergency. The crew asked for vectors to the Reno airport as their instrument panel was severely damaged by the impact. As the flight progressed north, they spotted an airport and asked air traffic controllers if the RNO airport was at their 11 o'clock. The controllers responded by indicating that the airport was at their 11 o'clock at 20 miles. The crew continued to the airport they observed (Carson City, Nevada, CXP) and elected to land.
As the flight neared CXP, the flight crew noted that the right engine shut down as a result of the impact. The flight crew entered a left downwind for runway 9 and the landing gear would not extend normally. The flight crew overshot final for runway 9 due to the terrain limiting the available length of the downwind leg and attempts to maintain an adequate airspeed to control the airplane. Then, they entered the downwind leg for runway 27. As the captain slowed the airplane for final approach she asked the first officer to assist in controlling the airplane's bank and pitch attitudes. The airplane touched down on the runway centerline, with the landing gear retracted, and came to rest uneventfully.
The airplane was equipped with a cockpit voice recorder (CVR), which recorded the captain and first officer's communications with air traffic control, and with one another, as they descended toward RNO. The last clearance received from Oakland ARTCC was for them to descend to flight level (FL) 220, then, at pilot discretion, maintain 16,000 feet. The captain and first officer then discussed the descent and/or approach, and at 1506:19, the CVR recorded a sound similar to a gasp on the captain's microphone followed by unusual electronic sounds. The recording ended at that point, at 1506:24.
1.1.2 Glider Pilot Statement
On the morning of the accident, the glider pilot received a flight review in a DG-505 glider and then flew his first flight in the accident glider. He started his second flight in the accident glider at 1300. He intended on thermal flying for about 5 hours and wanted to stay in the local area to familiarize himself with the accident glider. He flew around the local area and entered a thermal on the southwest side of Mt. Seagul. He entered a 30-degree left bank spiraling climb at 50 knots. During the climb, as the glider turned toward the south, the pilot saw a jet aircraft heading toward him. He estimated that one second passed between the time he noted the jet aircraft and the time they collided. He said he may have entered a slight nose down control input, but it wasn't enough to avoid the collision.
The Hawker jet impacted the right wing of the glider near the right outboard wing joint (the glider had a 4-piece wing with two inboard sections and two outboard sections). The glider entered a flat spin after the impact, so the pilot elected to remove the cockpit canopy and bail out. After removing the canopy, the pilot checked his ripcord location, unbuckled his restraint system, and bailed out of the glider. The pilot pulled the ripcord and the parachute successfully opened. During his descent, he observed the glider spiral to the ground below him and noted that the left wing and inboard section of the right wing remained attached to the fuselage. He landed uneventfully, but sustained minor injuries when the parachute dragged him along the ground. The pilot waited near his landing area for 1.5 hours before he began walking toward Carson Valley. After 2 hours and 10 minutes of walking along a dirt road, he was picked up by local authorities.
1.2 PERSONNEL INFORMATION
1.2.1 Hawker Flight Crew Information
The captain held an airline transport pilot certificate with a multi-engine airplane rating and type ratings in Cessna 500 and Hawker Siddeley HS-125 airplanes. She also held a commercial pilot certificate for single-engine airplanes. She was issued a first-class medical certificate on April 17, 2006, with no limitations. According to the Pilot/Operator Aircraft Accident Report (NTSB Form 6120.1/2) submitted by NetJets Aviation, Inc., the captain accumulated a total of 6,134 total flight hours, of which 1,564 hours were accrued in Hawker 800XP airplanes.
The captain was wearing sunglasses at the time of the event.
The first officer held an airline transport pilot certificate for multi-engine airplanes and type ratings in Beech 400, Hawker Siddeley HS-125, and Mitsubishi MU-300 airplanes. He also held a commercial pilot certificate for single-engine airplanes. He was issued a first-class medical certificate on May 16, 2006, with a limitation indicating he must wear corrective lenses. According to the 6120.1/2 Form, he accumulated 3,848 total flight hours, of which 548 hours were accrued in the Hawker 800XP.
The first officer was wearing corrective glasses, with sunshades clipped over the glasses, at the time of the event.
1.2.2 Glider Pilot Information
The glider pilot was a Japanese national, and had last flown in the Minden area in 2000. He held a private pilot certificate with a glider rating. He obtained the equivalent of a second-class medical certificate on June 20, 2006, from Japan's Civil Aeronautics Board; however, he did not hold a current FAA-issued medical certificate, nor was one required to act as pilot-in-command of a glider.
1.3 AIRCRAFT INFORMATION
1.3.1 Hawker 800XP Information
The Hawker 800XP was equipped with a Traffic Collision and Avoidance System (TCAS). TCAS is an airborne collision avoidance system based on radar beacon signals, which operates independent of ground-based equipment. TCAS-I generates traffic advisories only. TCAS-II generates traffic advisories, and resolution (collision avoidance) advisories (RA) in the vertical plane. For an aircraft equipped with TCAS to provide an RA, it must receive beacon information from the transponder installed on another local aircraft. The Hawker was equipped with the TCAS-II version, which would have provided a RA had it received a signal from another transponder.
1.3.2 Glider Information
The glider was equipped with a panel mounted communication radio, global positioning system (GPS) unit, a Cambridge 302, and a Mode C transponder; however, the pilot did not turn on the GPS and transponder. According to the glider pilot, he did not turn on the transponder because he was only intending on remaining in the local glider area, and because he wanted to reserve his batteries for radio use. The glider was equipped with two batteries (one main and one spare), however, due to the previous glider flights, the pilot was unsure of the remaining charge in the battery.
1.4 METEOROLOGICAL INFORMATION
At 1456, the weather observation facility located at RNO reported the following information: wind from 280 degrees at 11 knots with gusts to 17 knots, visibility 10 statute miles, a few clouds at 11,000 feet, temperature 34 degrees Celsius, dew point minus 04 degrees Celsius, and an altimeter setting of 30.01 inches of mercury.
1.5 COMMUNICATIONS
The Hawker 800XP was in radio communication with Oakland ARTCC and had just been handed off to the RNO Terminal Radar Approach Control (TRACON)...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX06FA277