N1949W

Substantial
None

Beech B19S/N: MB-610

Accident Details

Date
Friday, September 29, 2006
NTSB Number
CHI06CA274
Location
Pontiac, MI
Event ID
20061020X01547
Coordinates
43.665554, -83.420280
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The pilot's failure to perform a go-around when he noticed the airplane was not on a stabilized final approach. Contributing factors to the accident were the hard landing, the subsequent pilot-induced oscillation (porpoise) which resulted in the collapse of the nose landing gear, and the taxiway sign.

Aircraft Information

Registration
N1949W
Make
BEECH
Serial Number
MB-610
Engine Type
Reciprocating
Year Built
1973
Model / ICAO
B19BE19
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
WOITYRA MICHAEL J
Address
626 WESBROOK ST
Status
Deregistered
City
PONTIAC
State / Zip Code
MI 48340-3065
Country
United States

Analysis

The airplane porpoised during landing, which resulted in the collapse of the nose landing gear. The pilot stated that he noticed the airplane was "higher than normal and a little fast" during final approach and to correct he "added full flaps slowing down to the right speed, but noticed a faster descent rate." The pilot reported that he increased engine power to arrest the descent, but during the landing flare the airplane's nose "dropped and hit the runway first and ballooned the aircraft back into the air quite abruptly." The pilot stated that he "immediately applied full power for a go around ... the aircraft turned slightly to the right because of a slight crosswind, and there was not enough altitude to nose down and raise the flaps at the same time." The pilot reported that the airplane's nose "sharply dropped and hit the nose gear on the runway for a second time and broke off, hitting the prop and stopping the engine." The pilot stated that the airplane impacted a taxiway sign before coming to a stop. The pilot reported that the accident could have been prevented if he had initiated a go-around after noticing the airplane was not on a stabilized final approach.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI06CA274