N57RMPeay Quckie Q-2002007-02-17 NTSB Accident Report

Substantial
None

Peay Quckie Q-200S/N: 2699

Summary

On February 17, 2007, a Peay Quckie Q-200 (N57RM) was involved in an incident near Livermore, CA. All 1 person aboard were uninjured. The aircraft sustained substantial damage.

The National Transportation Safety Board determined the probable cause of this incident to be: The pilot failed to maintain directional control during an aborted takeoff.

The pilot reported that this was his first flight in the airplane. After liftoff the airplane would not climb, therefore, he decided to land the airplane from an altitude of 4 feet. The landing attempt resulted in a bounced landing. The airplane veered off the runway at 40 knots, traveled through muddy grass, and nosed over. The pilot stated that he misperceived the problem and did not apply the required control input force to effectively move the elevator, which would have resulted in greater pitch control.

This incident is documented in NTSB report LAX07CA096. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N57RM.

Accident Details

Date
Saturday, February 17, 2007
NTSB Number
LAX07CA096
Location
Livermore, CA
Event ID
20070305X00252
Coordinates
37.700000, -121.243614
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot failed to maintain directional control during an aborted takeoff.

Aircraft Information

Registration
Make
PEAY
Serial Number
2699
Engine Type
Reciprocating
Year Built
1988
Model / ICAO
Quckie Q-200
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
Q-200 A

Registered Owner (Current)

Name
ISBERG WESTON T
Address
15042 REYNOSA DR
City
RANCHO MURIETA
State / Zip Code
CA 95683-9143
Country
United States

Analysis

The pilot reported that this was his first flight in the airplane. After liftoff the airplane would not climb, therefore, he decided to land the airplane from an altitude of 4 feet. The landing attempt resulted in a bounced landing. The airplane veered off the runway at 40 knots, traveled through muddy grass, and nosed over. The pilot stated that he misperceived the problem and did not apply the required control input force to effectively move the elevator, which would have resulted in greater pitch control.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX07CA096