Summary
On April 12, 2007, a Cessna 172M (N9685Q) was involved in an accident near Stockton, CA. The accident resulted in 1 minor injury. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this accident to be: The loss of engine power due to fuel exhaustion resulting from the pilot's inaccurate fuel consumption calculations and failure to refuel while en route.
The pilot stated in the Pilot/Operator Accident Report that he departed El Monte, California, with both fuel tanks full of 100LL. His route of flight, El Monte to Stockton, California, usually takes 3 hours to fly. He encountered turbulence and strong winds, which had the effect of increasing the flight time to 4 hours. As he lined up for a straight-in approach to the Stockton Metropolitan Airport, the engine stopped due to fuel exhaustion. The pilot executed a forced landing short of the approach end of runway 29, which collapsed the nose gear and buckled the engine firewall.
This accident is documented in NTSB report LAX07CA125. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N9685Q.
Accident Details
Probable Cause and Findings
The loss of engine power due to fuel exhaustion resulting from the pilot's inaccurate fuel consumption calculations and failure to refuel while en route.
Aircraft Information
Registered Owner (Historical)
Analysis
The pilot stated in the Pilot/Operator Accident Report that he departed El Monte, California, with both fuel tanks full of 100LL. His route of flight, El Monte to Stockton, California, usually takes 3 hours to fly. He encountered turbulence and strong winds, which had the effect of increasing the flight time to 4 hours. As he lined up for a straight-in approach to the Stockton Metropolitan Airport, the engine stopped due to fuel exhaustion. The pilot executed a forced landing short of the approach end of runway 29, which collapsed the nose gear and buckled the engine firewall. The pilot stated that the airplane and engine had no mechanical malfunctions.
An FAA inspector examined the airplane at the accident scene and confirmed that there was no fuel onboard.
The airplane had been modified with the installation of a higher horsepower Lycoming O-360-A1A engine in place of the original O-320.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX07CA125