N851BP

Destroyed
Fatal

EUROCOPTER AS 350 B3S/N: 3588

Accident Details

Date
Tuesday, May 22, 2007
NTSB Number
DFW07GA119
Location
San Elizario, TX
Event ID
20070530X00664
Coordinates
31.579166, -106.284446
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
1
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The pilot's encounter with a vortex ring state and his inability to maintain control of the helicopter.

Aircraft Information

Registration
N851BP
Make
EUROCOPTER
Serial Number
3588
Year Built
2002
Model / ICAO
AS 350 B3

Registered Owner (Historical)

Name
US BORDER PATROL AIR OPERATIONS
Address
9C BUTTERFIELD TRAIL
Status
Deregistered
City
EL PASO
State / Zip Code
TX 79906
Country
United States

Analysis

History of Flight

On May 22, 2007 at 0838 mountain daylight time, a single-engine Eurocopter, AS350-B3 turbo-shaft helicopter, N851BP, registered to and operated by the U.S. Customs and Border Protection (CBP) Air Operations, was destroyed when it impacted terrain following a loss of control while maneuvering at approximately 150- above ground level and an airspeed between 20 to 30 knots on a routine border patrol mission near San Elizario, Texas, approximately 15 miles southeast of the El Paso International Airport. The accident occurred 1.8 hours in to the flight. The commercial pilot sustained fatal injuries and his non-rated observer was seriously injured. Visual meteorological conditions prevailed, and a company visual flight rules flight plan was filed for the local flight conducted as a Public Use Flight under 14 Code of Federal Regulations Part 91. The flight departed El Paso International Airport (KELP), near El Paso, Texas, at approximately 0655.

Local authorities reported that the helicopter impacted a parked pickup truck in a nose-low attitude while in a right turn, coming to rest on its right side in a residential area. There were no reported injuries to anyone on the ground. Emergency medical services personnel removed the pilot and observer from the cockpit and transported them to a local hospital.

Following the documentation of the wreckage, the helicopter was recovered to a secured facility at Biggs Army Airfield, near El Paso, Texas, for a detailed examination. The engine, transmission, and flight control hydraulic servos were removed and shipped to laboratory facilities for testing and/or teardown examination along with other drive train components.

Damage to Aircraft

Several witnesses were interviewed during the field portion of the investigation. Most witnesses concluded that the helicopter "appeared to dip the nose-down and enter a spin to the right nearly straight down. One witness stated that the helicopter appeared to have recovered from the spin and initiated a climb before it began to spin to the right again and impacted the ground in a near-vertical attitude. Other witnesses added that the engine appeared to be "screaming." Another witness, who reported having experience as a helicopter mechanic, added that the engine was screaming, but that the rotor system sounded as though it was slowing down. One witness stated it sounded like it was sucking or chopping air.

Injuries to Persons

The air transport rated pilot was killed. The observer sustained critical injuries.

Other Damage

A 1978 GMC pickup truck that was parked at the rear of the residence was destroyed. As the aircraft impacted the vehicle, the right skid of the helicopter struck the cab roof causing the top to collapse across the width of the body. The truck bed showed collision damage on both the forward end of the driver’s side and aft end of the passenger’s side. The tail gate was cut along its width when the helicopter’s main rotor struck the vehicle, and it was found hanging from the vehicle’s frame.

Personnel Information

The pilot held an Airline Transport Pilot certificate with single engine airplane, multi-engine airplane, helicopter, and instrument ratings. He joined the U.S. Customs and Border Patrol (CBP) Air and Marine in 1991 where he was assigned to the New York Air Unit and the Puerto Rico Air Operations Branch before transferring to the El Paso Air Branch in the summer of 1996. While at the El Paso Air Branch, the pilot received training in, and was eventually endorsed to fly the AS350-B3 aircraft as Pilot-In-Command. The pilot had accumulated a total of 3919 flight hours, of which 173 hours was in CBP AS350 aircraft.

Initial AS350 training for the pilot was conducted at the University of North Dakota, UND Aerospace, Grand Forks, North Dakota and completed on July 31, 1998. During that year, the pilot logged 19.7 hours of which 1.5 hours were as PIC. From 1999 until late 2003, the pilot accumulated an additional 11.2 hours in the AS350 with 4 hours as PIC. From 2003-2004, no records were discovered indicating the pilot had flown any additional AS350 hours. The next indication of flight time was in 2005 when he logged 22.6 hours as Second-In-Command. From January 01, 2006 to the accident in May 2007, the pilot amassed an additional 121 hours of which 62.7 hours were as PIC. On December 19, 2006, the pilot started AS350-B3 initial transition training at HeliStream located in southern California. On January 5, 2007 in El Paso, the AIA started CBP AS350-B3 transition training and completed said training on February 6, 2007. On February 28, 2007, the pilot was designated as a pilot in command and maintenance test pilot. All training and check rides were completed with satisfactory marks with no derogatory comments. CBP initial training and check ride were completed by the same instructor.

The Border Patrol Agent Observer joined CBP on February 23, 2003 and upon completing his academy training was assigned to the El Paso Sector in August 2003. In 2007, the agent volunteered as an observer with the Air and Marine program and was assigned flight duties as a Qualified Observer in May 2007. The Observer held a private pilot certificate for single engine land airplanes.

Aircraft Information

N851BP, serial number 3588, was purchased by U.S. Customs and Border Protection in April 2003 from American Eurocopter, Grand Prairie, TX. According to records, the aircraft was maintained in accordance with the manufacturer’s recommended procedures. Documentation indicated that the last major maintenance was performed May 18, 2007 by El Paso Aero, Inc., a licensed, FAA-certified repair facility. The maintenance was a 100-hour airframe inspection in accordance with the US CBP Inspection Program and AS350-B3 Master Service Recommendations. Maintenance procedures were completed with no discrepancies noted.

N851BP had a Turbomeca Arriel 2B1 engine producing 848 horsepower that was installed on the aircraft 941.9 hours prior to the accident. The engine had 941.9 total hours and the airframe had 3843.8 hours. Work cards for the aircraft showed that there were no major discrepancies outstanding on the airframe prior to departure and that all major Airworthiness Directives had been complied with.

Weight and balance calculations confirmed that the aircraft was within maximum weight allowances and within center of gravity limits at the time of departure. The aircraft was fueled with approximately 100 gallons of Jet A making the aircraft weight approximately 4357 pounds at time of takeoff. After flying for 1.8 hours, at the estimated time of impact, the aircraft would have weighed 3709.9 pounds and the Center of Gravity would have been 130.7 inches aft of datum.

Meteorological Information

At 0851 MDT, the weather reporting facility at the El Paso International Airport (KELP) reported wind from 260 degrees at 12 knots, visibility 10 statute miles, clear skies, temperature 23 degrees Celsius, dew point 1 degree Celsius, and a barometric pressure of 29.94 inches of Mercury. Density Altitude was computed to be 5433 feet MSL, Pressure Altitude 3941 feet based on these conditions and a terrain level of 3645 feet MSL at the accident site.

Flight Recorders

No flight recorders were installed on this helicopter.

Wreckage and Impact Information

The fuselage came to rest on its right side in the back yard of a residence, adjacent to a parked truck. A large portion of the tailboom had separated and came to rest on the bed of the truck. Rotational damage consistent with the size and dimensions of the tail rotor strike tabs was observed on the left side of the truck.

A detailed examination of the wreckage was conducted at Biggs Army Airfield, El Paso, Texas. Impact damage to cabin and fuselage, deformation of the transmission deck and displacement of the main transmission, as well as deformation of the energy attenuating seats evidenced a right side impact.

The blue and red star arms of the Starflex rotor head were fractured approximately mid-span at 45-degree angles. The yellow star arm was broken inward of the star arm bushing and exhibited broom straw of the composite fibers. All three blade sleeves exhibited impact damage. All three rotor blades exhibited impact damage on the leading edges; trailing edge splitting and chord wise bending was also observed.

The engine to transmission drive shaft separated at the transmission input flex coupling. The main transmission input flex coupling shattered and exhibited splaying.

Two of the three transmission input flange bolts remained attached with portions of the flex coupling still attached. The linking tube exhibited rotational scoring.

The main transmission appeared in good condition, but did not rotate at the recovery site; it was retained for further examination. Three of the four transmission support bars were separated and exhibited angular fracture surfaces.

The rotor brake and fuel cutoff levers were found in the forward/stowed position. The hydraulic cutoff switch was in the on (normal/guarded) position; the upper surface of the guard was broken. The collective(s) was found in a nearly full up position; the cyclic(s) was in a right lateral input position; anti-torque pedals were found with left pedal input (forward). Main rotor control continuity was confirmed; all hardware was found intact.

The hydraulic system pump and pulley assembly with black poly-v belt was intact. The hydraulic reservoir contained fluid. The 3-micron hydraulic filter clogging indicator, which is designed to extend at a delta pressure of 2.7 bars (39.16 psi), was found extended. A hydraulic fluid sample was taken by CBP and sent to the U.S. Army for analysis. Test results revealed the sample contained higher than PPM level of water and possibly hydraulic fluids mixed with MIL-23699. The hydraulic servos were retained for further examination at ...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# DFW07GA119