Accident Details
Probable Cause and Findings
Carburetor icing, which resulted in a loss of engine power. Also causal, was the pilots' failure to maintain airspeed during the forced landing, which resulted in an inadvertent stall.
Aircraft Information
Registered Owner (Historical)
Analysis
HISTORY OF FLIGHT
On June 21, 2007, about 1150 eastern daylight time, a Cessna 182C, N8691T, was destroyed when it impacted terrain at Gryder-Teague Airport (NC58), Hiddenite, North Carolina. The certificated private pilot/owner and the certificated flight instructor were fatally injured. Visual meteorological conditions prevailed, and no flight plan was filed for the local flight, which departed Taylorsville Airport (4NC3), Taylorsville, North Carolina. The instructional flight was conducted under 14 CFR Part 91.
According to relatives, the flight was intended as training for the pilot/owner. A notation in the pilot's logbook, for a flight 1 day earlier, stated, "Instrument (illegible) Instructor."
There were no witnesses to the accident, and the extent to which a preflight inspection was performed was unknown.
According to a representative from the Air Force Rescue Coordination Center, the airplane's emergency locator transmitter signal was received by a satellite at 1150, and notification from the satellite occurred at 1204.
PERSONNEL INFORMATION
According to Federal Aviation Administration (FAA) records, the pilot/owner, age 75, held a private pilot certificate. His latest FAA third class medical certificate was issued on July 18, 2005. The pilot/owner's logbook indicated that he had accumulated 279 hours of flight time.
The flight instructor, age 70, held an airline transport pilot certificate for airplane multiengine land, a commercial certificate for airplane single-engine land and single-engine sea, and was rated in a number of transport category airplanes. He also held a flight instructor certificate for single-engine and multiengine airplanes, and instrument airplane, and was a retired airline pilot. Accurate flight hours were not available. The instructor's latest FAA second class medical certificate was issued on May 15, 2006.
AIRCRAFT INFORMATION
FAA records indicated that the airplane was manufactured in 1960, and powered by a Teledyne Continental Motors (TCM) O-470 engine. The airplane was not equipped with a carburetor temperature gauge.
A review of maintenance records revealed that on May 17, 2007, the airplane underwent an annual inspection at a facility at Statesville Regional Airport. At that time, the tachometer indicated 953.88 hours.
On May 18, 2007, the pilot had the airplane topped off with 41.5 gallons of fuel and then flew it back to Taylorsville. At the end of the flight, the pilot/owner logged a tachometer time of 954.25 hours.
On June 20, 2007, after the instrument training flight, the pilot/owner noted a tachometer time of 955.09 hours.
At the accident site, the tachometer time indicated 955.61 hours.
AIRPORT INFORMATION
Gryder-Teague Airport, which was surrounded by trees in the vicinity of the accident, had one turf runway, runway 27, which was 2,000 feet long and 60 feet wide. Airport elevation was 1,190 feet and there was no control tower.
METEOROLOGICAL INFORMATION
Weather, recorded at an airport 13 nautical miles to the southeast, at 1147, included clear skies, visibility 10 statute miles, and winds from 030 degrees true at 4 knots. The temperature was 27 degrees Centigrade (80 degrees Fahrenheit) and dew point was 7 degrees Centigrade (45 degrees Fahrenheit). Relative humidity was 28 per cent.
WRECKAGE AND IMPACT INFORMATION
The main wreckage was located about 80 feet south of runway 27, approximately 200 feet beyond the threshold, in the vicinity of 35 degrees, 55.10 minutes north latitude, 81 degrees, 06.85 minutes west longitude.
An examination of the runway 27 approach area revealed that several small, less than 1-inch-diameter branches were separated from a tree about 150 feet to the east. The estimated height of tree damage was 60 to 70 feet above the runway.
Clear plastic landing light fairing fragments were found on the runway approximately 20 feet beyond the threshold. A ground scar, containing red plastic lens material, commenced about 15 feet south of the runway edge, about 130 feet beyond the threshold. The scar and wreckage path were aligned along a 265-degree magnetic heading.
An impact crater was located along the path, approximately 160 feet beyond the runway threshold, and about 10 feet beyond that, was the propeller hub, with the propeller blades still attached. Two of the three propeller blades had no leading edge damage. A third blade had leading edge damage, and fit exactly into a cut into the ground. A small section of that blade was also found in the cut.
The spinner had aft crush damage, with no rotational scoring or crushing. The bolt holes for joining the propeller hub to the engine attach studs displayed some radial elongation, with no rotational elongation or scoring.
The main wreckage was located about 40 feet beyond the propeller hub. The airplane was resting on its nose, at an approximately 60-degree nose-down angle, with its tailcone supported by a tree. The aft fuselage was angled about 30 degrees toward the left wing. The outboard half of the right wing was crushed aft, with uniformly increasing crush further outboard. The left wing also had leading edge crush, but it was not uniform along the wing.
All flight control surfaces were accounted for at the accident scene. Control cable continuity was confirmed from all flight control surfaces to the cabin area. The flaps were fully retracted, and the manual flap handle was stowed in a position corresponding to the flaps being fully retracted.
Fresh fuel stains were noted on the tops of the wings. The right fuel tank was not breached, and trace amounts of fuel were inside. There was some browning of vegetation below the right wing. The left fuel tank was breached, but still had 2 to 3 inches of fuel in the forward portion of the nose-low tank. The gascolator was destroyed and the fuel line was compromised. The carburetor bowl was less than 1/4 full.
In the cockpit, the mixture and propeller controls were found in the full forward position. The throttle was also in the full forward position, but bent to the left, and the "CARB HEAT PULL HOT" knob was all the way in.
Engine crankshaft and valve train continuity was confirmed, as was compression in all cylinders. Spark plug electrodes were dark gray in color. Both magnetos were tested, with spark achieved on seven of the eight leads. One lead was separated.
The carburetor was found partially separated from the engine, and displayed impact damage. The throttle lever and the throttle positions were consistent with "full open," and the mixture control lever was in the "full rich" position. The throttle and mixture levers moved freely from stop to stop by hand. The carburetor was disassembled, during which, the gasket was damaged when it stuck to the two mating surfaces. There was no debris within the carburetor, and the about 1/2 inch of blue liquid, consistent in appearance and odor with 100LL fuel, was found in the carburetor bowl.
The engine was subsequently forwarded to the manufacturer's facilities in Mobile, Alabama, for further testing, and on November 6, 2007, an engine test run was performed under FAA oversight. According to the Operational Test Report, the carburetor, which had previously been disassembled for examination at the accident site, was reassembled and reinstalled on the engine prior to the test. The engine was then moved to a test cell, and experienced a "normal" start on the first attempt. The engine was then advanced in rpm steps, and allowed to stabilize for 5 minutes at each step. Maximum rpm attained during full throttle was 2,400. Throughout the test, the engine exhibited "hesitation."
The original carburetor was subsequently replaced with a serviceable unit, and during the test run, attained 2,680 rpm, "without any hesitation, stumbling or interruption in power."
The report also noted that there was a "damaged and incomplete gasket installed" with the original carburetor, which would have precluded normal operation and rated horsepower.
MEDICAL AND TOXICOLOGICAL INFORMATION
Local authorities released the pilots' remains without performing autopsies, which precluded FAA comprehensive toxicological testing. Local authorities did provide single-source blood samples from each pilot to the North Carolina Medical Examiner's Office, which were only tested for, and were negative for, ethanol.
The Medical Examiner also determined that the probable cause of death for both pilots was "multiple trauma."
ADDITIONAL INFORMATION
According an article on the Cessna Flyer Association website titled "The Cessna 182":
"The 182 aircraft in general are prone to carburetor icing, so the carb heat must be fully operational and turned on in advance of the need to actually use it."
According to an article on the Cessna Pilots Association website titled "1956 through 1986 Cessna 182 Fixed Gear Skylane Buyers Guide Excerpt":
"The Cessna 182 Skylane is prone to developing carburetor ice. The reason for this is because the design of the induction system has the carburetor positioned well below the engine in the cowling and away from the warm air around the engine. Because of this tendency towards carburetor ice many Cessna 182 Skylanes were delivered with a carburetor temperature gauge. The Cessna Pilots Association has strongly recommended to its members that they utilize carburetor heat in such a manner as to keep the carburetor temperature indication out of the yellow zone of the gauge."
FAA Advisory Circular 20-113, "Pilot Precautions and Procedures to be Taken in Preventing Aircraft Reciprocating Engine Induction System and Fuel System Icing Problems" includes several carburetor icing considerations:
"Throttle Ice - Throttle ice is usually formed at or near a partially closed throttle, typical of an off-idle or cruise power setting. This occurs when water vapor in the air condenses and freezes because of the cooling restriction caused by the carburetor venturi and the throttle butterfly v...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# NYC07FA145