N44118

MINR
Serious

Powrachute Corp. Pegasus 912MS/N: E007PC

Accident Details

Date
Saturday, July 28, 2007
NTSB Number
MIA07LA130
Location
Suffolk, VA
Event ID
20070814X01187
Coordinates
36.692501, -76.603332
Aircraft Damage
MINR
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The improper installation of the engine oil filter. A factor contributing to the accident was unsuitable terrain for a forced landing.

Aircraft Information

Registration
N44118
Make
POWRACHUTE CORP.
Serial Number
E007PC
Year Built
2004
Model / ICAO
Pegasus 912M

Registered Owner (Historical)

Name
XTREME ADVENTURES INC
Address
2140 MARINA SHORES DR
Status
Deregistered
City
VIRGINIA BEACH
State / Zip Code
VA 23451-6800
Country
United States

Analysis

On July 28, 2007, about 0713 eastern daylight time, a Powrachute Pegasus 912M, powered parachute, N44118, registered to Xtreme Adventures, Inc. and operated by an individual, had a loss of engine power and impacted into a tree after takeoff from Suffolk Executive Airport (SFQ), Suffolk, Virginia. Visual meteorological conditions prevailed at the time and a visual flight plan (VFR) flight plan was filed for the 14 CFR Part 91 personal flight. The pilot received serious injuries and the aircraft incurred minor damage. The flight originated about 0700.

The pilot stated that during the climb, at 1,800 feet, he observed a 1,000 rpm drop in engine power. He elected to return to SFQ, and several seconds later the engine seized abruptly. The pilot looked for a field for the force landing. During the descent, at 300 feet, he was aligned on to a road. All of a sudden three people and a dog appeared on the road and were not moving from their position. He elected to turn left and head toward an oak tree. The aircraft impacted the tree, dropped straight down, and landed hard in the upright position.

During post recovery examination of the aircraft by a Federal Aviation Administration inspector it was reveal that the engine seized due to lack of engine oil. The oil leak was observed from the engine oil filter, which had been changed about 9 hours before the accident flight during schedule maintenance. The oil filter was examined by a Rotax Aircraft Engines representative with National Transportation Safety Board oversight. The examination revealed that the oil filter attaching thread were consistent with over torque scoring. The Rotax's maintenance manual instructs mechanics to "screw the oil filter on by hand until it stops at the filter house, then tighten an extra 3/4 turn."

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA07LA130