N39YP

Substantial
Fatal

Clifford Titan Tornado IIS/N: D00912SOHK0365

Accident Details

Date
Friday, August 17, 2007
NTSB Number
CHI07LA272
Location
Henning, MN
Event ID
20070817X01200
Aircraft Damage
Substantial
Highest Injury
Fatal
Fatalities
1
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The inadvertent stall and low airspeed while maneuvering. A contributing factor was the low altitude of the maneuver.

Aircraft Information

Registration
N39YP
Make
CLIFFORD
Serial Number
D00912SOHK0365
Engine Type
Reciprocating
Year Built
2002
Model / ICAO
Titan Tornado IIBPAT
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
HESCHKE CLIFFORD
Address
29420 435TH AVE
Status
Deregistered
City
OTTERTAIL
State / Zip Code
MN 56571-9667
Country
United States

Analysis

On August 16, 2007, at 2023 central daylight time, an experimental amateur-built Titan Tornado II, N39YP, piloted by a private pilot, received substantial damage on impact with terrain while maneuvering near a house about three miles north of Henning, Minnesota. Visual meteorological conditions prevailed at the time of the accident. The 14 CFR Part 91 personal flight was not operating on a flight plan. The pilot was fatally injured. The local flight originated from a private airstrip at 1930.

A witness stated that the airplane was headed in a northerly direction when it flew over a house and began turning to the west. The turn continued toward a southwesterly direction at which time the witness lost sight of the airplane. The witness stated that as the airplane was banking from the west and heading southeast, he heard the steady drone followed by a spike in engine noise. After the engine accelerated sharply, he heard nothing for a few seconds and then heard the crash. The witness stated that he was not sure of the airplane’s altitude, but the pilot had flown low over the house numerous times in the past to say hello.

Another witness reported that the airplane was flying low comparing it to a "crop duster." The airplane turned to the east followed by an increase in engine speed when it "twisted" while descending "straight down" impacting the ground.

Examination of the airplane by the Federal Aviation Administration revealed that the propeller was separated mid span and was resting about 15 feet behind the tail of the airplane. The airplane wing exhibited a slash mark consistent with a propeller strike. No anomalies were noted that would have precluded normal airplane operation.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI07LA272