Summary
On November 03, 2007, a Bellanca 7GCBC (N712j) was involved in an incident near Arcola, TX. All 2 people aboard were uninjured. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this incident to be: The loss of control as result of the pilot's failure to compensate for existing wind conditions while landing. A contributing factor was the gusty crosswind.
The private pilot lost control of the tailwheel-equipped airplane when he encountered a gust of wind from the right while attempting to land on Runway 27. Before the tailwheel contacted the ground, the tail moved left from the gust of wind causing the airplane to turn into the wind. The pilot was unable to compensate for gust of wind and lost control of the airplane. An attempt to execute a go-around was unsuccessful, and the airplane drifted off the 100-foot wide asphalt runway. The airplane contacted standing water in a nearby ditch, nosed over, and came to rest in the inverted position. The pilot reported the winds were from 290 degrees at 9 knots, gusting to 12 knots. The pilot reported having accumulated a total of 14-hours in the same make and model airplane.
This incident is documented in NTSB report DFW08CA023. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N712j.
Accident Details
Probable Cause and Findings
The loss of control as result of the pilot's failure to compensate for existing wind conditions while landing. A contributing factor was the gusty crosswind.
Aircraft Information
Registered Owner (Historical)
Analysis
The private pilot lost control of the tailwheel-equipped airplane when he encountered a gust of wind from the right while attempting to land on Runway 27. Before the tailwheel contacted the ground, the tail moved left from the gust of wind causing the airplane to turn into the wind. The pilot was unable to compensate for gust of wind and lost control of the airplane. An attempt to execute a go-around was unsuccessful, and the airplane drifted off the 100-foot wide asphalt runway. The airplane contacted standing water in a nearby ditch, nosed over, and came to rest in the inverted position. The pilot reported the winds were from 290 degrees at 9 knots, gusting to 12 knots. The pilot reported having accumulated a total of 14-hours in the same make and model airplane.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# DFW08CA023