N26WR

Substantial
None

Costruzioni Aeronautiche P2002 SierraS/N: 144

Accident Details

Date
Thursday, January 3, 2008
NTSB Number
MIA08LA034
Location
Stevensville, MD
Event ID
20080115X00046
Coordinates
38.972499, -76.324447
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A loss of engine power due to the failure of company maintenance personnel to comply with engine manufacturers requirements for carburetor adjustment during the 100-hour inspection.

Aircraft Information

Registration
N26WR
Make
COSTRUZIONI AERONAUTICHE
Serial Number
144
Year Built
2005
Model / ICAO
P2002 Sierra

Registered Owner (Historical)

Name
CSP LEASING LLC
Address
8095 AIRPORT RD
Status
Deregistered
City
LAUREL
State / Zip Code
DE 19956-4218
Country
United States

Analysis

On January 3, 2008, at 1545 eastern standard time, a Costruzioni Aeronautiche Techna P2002 Sierra, certificated Light Sport airplane, N26WR, lost engine power during final approach and collided with the ground during the subsequent forced landing, at the Bay Bridge Airport (W29), Stevensville, Maryland. The airplane was substantially damaged. The commercial pilot was not injured. Visual meteorological conditions prevailed for the personal flight. The airplane was registered to and operated by CSP Leasing LLC under the provision of Title 14 Code of Federal Regulations Part 91. The flight originated from W29 at 1440.

The pilot stated that during approach to W29 he reported downwind, base, and then final to runway 29. At about 100 feet above ground level he reduced the engine power to idle and subsequently lost engine power. He then made an emergency landing in a field short of runway 29.

Examination of the airplane by a Federal Aviation Administration inspector, and the engine's manufacturer revealed that there were 10 gallons of AVGAS in the wing tanks. During the examination of the engine the mechanical settings of the carburetor mixture and throttle stop were found to be out of adjustment. According to the Rotax maintenance manual the carburetor adjustments and synchronization should be checked at the 100-hour inspection. Review of the engine maintenance logbook revealed that the 100-hour inspection was conducted on December 17, 2007 at a Hobbs and total time of 113.4 hours, 19 flight hours before the accident. There were no recorded entries of the carburetor inspection or adjustment.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA08LA034