Accident Details
Probable Cause and Findings
The pilot's loss of control due to spatial disorientation and the pilot exceeding the design/stress limits of the aircraft. Factors contributing to the accident were the pilot's reported gyro problem, the dark night conditions , and prevailing instrument meteorological conditions.
Aircraft Information
Registered Owner (Historical)
Analysis
HISTORY OF FLIGHT
On January 16, 2008, at 2043 central standard time, a twin-engine Aero Commander 500-B airplane, registered as N712AT, was destroyed during an in-flight break-up and subsequent impact with terrain following a loss of control after take-off from Runway 36L at the Tulsa International Airport, near Tulsa, Oklahoma. The commercial pilot, sole occupant of the airplane, was fatally injured. The airplane was registered to and operated by Central Air Southwest, Inc., of Kansas City, Missouri, and was being utilized as an on demand air-carrier flight, hauling canceled bank checks. Dark night instrument meteorological conditions prevailed in the area at the time for the cargo flight conducted under 14 Code of Federal Regulations Part 135. An instrument flight rules flight plan had been filed and activated for the 94-nautical mile night cross-country flight from the Tulsa International Airport (TUL) to the Wiley Post Airport (PWA), near Oklahoma City, Oklahoma.
Authorities at the airport reported that soon after departing TUL, the pilot reported that he was having gyro problems. The airplane was observed on radar and was given instructions to turn left to 300 degrees. The pilot initiated a right turn and was informed by Tulsa approach control that "you are turning right, turn left to 300 degrees." The aircraft continued a steep right turn for two complete 360 degree turns and disappeared from the radar scope. The wreckage of the airplane was located about 90 minutes after the accident in a remote wooded area of Mohawk Park, approximately 1 3/4 miles north of the airport. There was no fire.
INJURIES TO PERSONS
The pilot was fatally injured. There were no injuries to anyone on the ground.
DAMAGE TO AIRCRAFT
The wreckage of the twin-engine airplane was located about 90 minutes after the accident in a remote wooded area of Mohawk Park, approximately 1.75 miles north of the airport (010 degrees from the departure end of the runway). There was no post-impact fire.
PERSONNEL INFORMATION
The 31-year old instrument rated pilot held a commercial certificate for single and multi-engine land airplanes. His last first class medical certificate was issued on November 19, 2007. The operator reported that the pilot had accumulated a total of 4,373-flight hours, of which 695-hours were in the same make and model aircraft. Additionally, the pilot was reported to have accumulated 255-hours in the preceding 90-days, with l83 in the last 30 days. The pilot's last biennial flight review was completed on November 29, 2007, in an Aero Commander 500-B.
The operator reported that the pilot was very familiar with the airplane and he had completed the scheduled flight almost on a daily basis since he joined the company.
AIRCRAFT INFORMATION
The 1961-model Aero Commander 500-B, serial number 1118-68, was reported to have accumulated a total of 17,888-flight hours at the time of its last inspection on January 10, 2008. The airplane has a maximum takeoff weight of 6,750-pounds, and the weight of the airplane at the time of takeoff from Tulsa was estimated at 6,005-pounds.
The aircraft was powered by two-290-horsepower IO-540-B1A5 Lycoming engines. The number one engine (left), serial number L-154-48, had accumulated a total of 126-hours since its last overhaul. The number two engine (right), serial number RL-7521-48, had accumulated a total of 1,276-hours since its last overhaul.
METEOROLOGICAL INFORMATION
The weather at the TUL airport at the time of the accident was reported as, a broken ceiling at 600 feet, an overcast ceiling at 1,900 feet, visibility 3 miles in rain and snow, temperature 31 degrees Fahrenheit, with winds from 300 degrees at 18 knots, gusting to 24 knots. The pilot was reported to have received a weather briefing for the flight.
COMMUNICATIONS
The Tulsa Air Route Traffic Control Center (ARTCC) personnel reported that at 45 seconds into the flight the pilot of N712AT, was cleared to climb to 6,000-feet and was given a left turn to a heading of 250-degrees, and cleared direct to PWA. The accident pilot acknowledged this transmission. At 1 minute and 59 seconds into the flight the controller noted that N712AT was in a right turn. At 2 minutes and 55 seconds the controller requested N712AT to report the altitude he was leaving and the pilot responded "3,500 I think I have lost my gyros, I'm trying to level out now". The controller responded "roger, you just made a right 360," to which the pilot responded "roger." At 3 minutes and 23 seconds after departure, the controller transmitted "712AT, you still appear to be in a right turn," to which the pilot responded "yeah, I'm having some trouble right now." At 3 minutes and 54 seconds the controller transmitted "712AT, I'm not getting a target on you, say altitude now." No response was received from the accident aircraft, and the accident airplane had disappeared from the radar scope. No further transmissions were received by the Tulsa ARTCC personnel.
WRECKAGE AND IMPACT INFORMATION
Examination of the aircraft wreckage was conducted at the accident site on January 18, 2008. The fractures were photographed and visually examined with a 10x magnifier and a high intensity light.
The first piece of aircraft wreckage along the debris field was the outboard portion of the left wing. The left wing was perched at a 45 degrees angle between two trees preventing extensive examination at its final resting place of North 36 degrees 13 minutes 7.51 seconds, West 95 degrees 53 minutes 4.46 seconds per the Tulsa Fire Department (TFD). All fractures of the wing structure (spars, longerons, and ribs) and wing skin were typical of ductile overload with no evidence of preexisting failures such as fatigue or stress-corrosion. Overall deformation of the wing indicated failure upward due to positive loading.
The second piece of the aircraft wreckage found was the outboard portion of the right wing. The right wing was resting in a pile of broken tree limbs preventing extensive examination at its final resting place of North 36 degrees 13 minutes 8.54 seconds, West 95 degrees 53 minutes 5.54 seconds per the TFD. All fractures of the wing structure (spars, longerons, and ribs) and skin were typical of ductile overload with no evidence of preexisting failures such as fatigue or stress-corrosion. Overall deformation of the wing indicated failure upward due to positive loading.
The empennage was found at North 36 degrees 13 minutes 8.64 seconds, West 95 degrees 53 minutes 5.74 seconds. The empennage was resting upright on its tail cone and its left and right horizontal stabilizer tips. The empennage separated from the aircraft at the fuselage-empennage junction just forward of the vertical stabilizer. All fractures of the fuselage-empennage structure (stringers) and skin were typical of ductile overload with no evidence of preexisting failures such as fatigue or stress-corrosion. Overall deformation of the fuselage-empennage junction indicated failure to the starboard side. The leading edges of the vertical stabilizer and the left horizontal stabilizer contained mechanical damage due to impact with the outboard portion of the right wing (detailed later). The bottom surface of the left horizontal stabilizer contained torsion buckles forward-aft indicating upward loading and the bottom surface of the right horizontal stabilizer contained torsion buckles aft-forward indicating downward loading. The left horizontal stabilizer upward loading and the right horizontal stabilizer downward loading indicates rolling of the aircraft from left to right which is characteristic of an in-flight breakup due to the right wing failing first.
The rudder was found approximately 20 yards north of the empennage. The rudder was fractured and folded in half. All the fractures of the rudder structure and skin were typical of ductile overload with no evidence of preexisting failures such as fatigue or stress-corrosion. The rudder control cable (multi-strand spiral wound steel cable, encased in a protective dual spiral wound steel strip, and covered with a fiber reinforced protective coating) was failed and noted to have been in less than ideal condition (airworthy). The multi-strand spiral wound steel cable failed approximately 8 inches from the rudder. The failure mode could not be determined without the aid of a stereo/scanning electron microscope. The cable was uniformly rusted due to an apparent failure of the fiber reinforced protective coating in service. The protective dual spiral wound steel strip was pulled unwound approximately 3-feet in length due to the in-flight breakup of the aircraft. The protective strips were uniformly rusted like the cable due to an apparent failure of the fiber reinforced protective coating in service. The fiber reinforced protective coating was cracked in numerous places.
The fuselage/main body of the airplane came to rest at North 36 degrees 13 minutes 9.00 seconds, West 95 degrees 53 minutes 6.16 seconds on a magnetic heading of 343 degrees. The fuselage/main body of the aircraft was found in the inverted position and was pancaked into the soft terrain to a height of approximately 2-feet preventing extensive examination at its final resting place. Front to rear it consisted of the nose to approximately BS 292 and left to right it consisted of approximately LWS145 to RWS 98. All of the readily observable fractures of the left and right wing and empennage structures and skins were typical of ductile overload with no evidence of preexisting failures such as fatigue or stress-corrosion. It should be noted that a majority of the fractures could not be visually examined on site due to pancaking into soft terrain.
Following visual examination of the outboard portions of the left and right wings at their final resting places, both wings were moved to a more suitable location for further examination. Over...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# DFW08FA056