N248DW

Substantial
Minor

Waltermire GlastarS/N: 5571

Accident Details

Date
Saturday, January 19, 2008
NTSB Number
LAX08CA048
Location
Vacaville, CA
Event ID
20080220X00213
Coordinates
38.377777, -121.961669
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
1
Total Aboard
2

Probable Cause and Findings

The pilot's failure to maintain directional control during landing and a lack of experience in conventional gear airplanes.

Aircraft Information

Registration
N248DW
Make
WALTERMIRE
Serial Number
5571
Engine Type
Reciprocating
Year Built
2003
Model / ICAO
GlastarBPAT
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
WALTERMIRE RICHARD D
Address
3221 LA QUINTA CT
Status
Deregistered
City
FAIRFIELD
State / Zip Code
CA 94534-7122
Country
United States

Analysis

On January 19, 2008, about 1300 Pacific standard time, a Waltermire Glastar, N248DW, swerved off runway 02 during landing at the Nut Tree Airport, Vacaville, California. The experimental homebuilt airplane was equipped with conventional (tail wheel) landing gear, and after exiting the runway it went into a ditch. The airplane's right wing and engine separated from the fuselage. The airplane was substantially damaged. The commercial certificated pilot was not injured. The passenger received a minor injury. The flight was performed under the provisions 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed at the time of the personal flight, and no flight plan was filed. The flight originated from Vacaville about 1200.

The pilot reported to the National Transportation Safety Board investigator that he intended to fly the airplane around the traffic pattern. The airplane bounced on the runway during the first two attempted landings, whereupon he applied engine power and performed go-arounds.

The pilot reported that he lost directional control of the airplane during the third attempted landing. While attempting to regain control he applied full engine power and overcorrected while manipulating the flight controls. His efforts at regaining control were not successful.

The pilot also reported that his experience flying the accident model of airplane was about 3 hours. The pilot acknowledged that he did not have a logbook endorsement to fly tail wheel equipped airplanes. The pilot reported that no mechanical malfunction was experienced during the flight. He stated to the Safety Board investigator that the accident was "just my fault."

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX08CA048