N473GF

Substantial
None

Cessna 305-AS/N: 2018

Accident Details

Date
Thursday, February 14, 2008
NTSB Number
LAX08LA060
Location
Mokuleia, HI
Event ID
20080516X00689
Coordinates
21.579444, -158.197219
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The failure of the left main landing gear strut due to fatigue. Contributing to the failure was the side load placed on the landing gear while making a crosswind landing.

Aircraft Information

Registration
Make
CESSNA
Serial Number
2018
Engine Type
Reciprocating
Year Built
1967
Model / ICAO
305-A
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
305A

Registered Owner (Current)

Name
HONOLULU SOARING CLUB INC
Address
PO BOX 626
City
WAIALUA
State / Zip Code
HI 96791-0626
Country
United States

Analysis

On February 16, 2008, at 1245 Hawaiian standard time, a Cessna 305-A, N473GF, experienced a left main landing gear collapse during a crosswind landing at Dillingham Airfield, Mokuleia, Hawaii. The airplane was operated by the Honolulu Soaring Club under the provisions of 14 Code of Federal Regulations (CFR) Part 91. The airline transport certificated pilot was not injured, and the airplane was substantially damaged. Visual meteorological conditions prevailed, and no flight plan had been filed. The local flight originated at Dillingham Airfield at 1230.

The pilot reported that he observed the windsocks at each end of runway 8/26, and both indicated tail winds of about 10 knots in either direction. The midfield windsock indicated a direct crosswind from the north. He elected to approach runway 8 and touched down abeam the midfield windsock. Upon touchdown the airplane experienced a left-to-right crosswind, and as the airplane decelerated, the pilot noticed the wind shift to a quartering right tail wind. He elected to execute a go-around. As he advanced the throttle, the engine sputtered, the left main landing gear collapsed, and the airplane ground looped to the left as it approached the runway's edge.

A Federal Aviation Administration inspector examined the left main landing gear spring strut and found that the strut separated where the wheel bolts to the strut. The fracture face of the strut was granular in texture and uniform matte gray in color. When the fracture surface of the landing gear strut section that remained attached to the wheel was more closely examined, it exhibited an approximate 1/16 inch flat dark triangular section at the corner of the mounting bolt hole. The Safety Board Materials Laboratory examination confirmed the presence of a 0.072 inch fatigue crack at this location.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX08LA060