N99180

Substantial
None

Ercoupe (Eng & Research Corp.) 415-CS/N: 1803

Accident Details

Date
Thursday, May 15, 2008
NTSB Number
LAX08LA142
Location
Penngrove, CA
Event ID
20080523X00719
Coordinates
38.299720, -122.666389
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The loss of engine power resulting from frayed magneto "P" leads, which shorted out and killed the ignition system. Contributing to the accident was the lack of suitable terrain for the forced landing.

Aircraft Information

Registration
Make
ERCOUPE (ENG & RESEARCH CORP.)
Serial Number
1803
Engine Type
Reciprocating
Year Built
1946
Model / ICAO
415-CERCO
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
415-C

Registered Owner (Current)

Name
RILLING NORMAN I JR
Address
201 A ST
City
BAKERSFIELD
State / Zip Code
CA 93304-2721
Country
United States

Analysis

On May 15, 2008, about 1510 Pacific daylight time, an Ercoupe 415-C, N99180, sustained substantial damage during a forced landing following a loss of engine power in Penngrove, California. The sport pilot and his passenger were not injured. The airplane was being operated by the pilot under Title 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed, and no flight plan was filed. The local personal flight departed from the Petaluma Municipal Airport, Petaluma, California, about 1450.

According to Sonoma County Sheriff's Department personnel, the pilot reported that while in cruise flight he noticed the oil pressure gauge begin to fluctuate erratically. The needle on the gauge "began to bounce up and down," and seconds later, the engine "began to cut out and sputter." The pilot headed back towards Petaluma Airport. However, the engine lost total power, and the pilot executed a forced landing in an alfalfa field about 4.5 miles northwest of the airport. During the landing roll in the 2- to 3-foot-tall grass, the airplane skidded sideways and the tail dug into the ground. The airplane's tail cone was buckled, and the right vertical stabilizer and rudder were bent.

The airplane was examined by Federal Aviation Administration (FAA) inspectors. The inspectors found that both magnetos had frayed primary wires ("P" leads) at the magnetos, which could have been shorting out and intermittently killing the ignition system. They noted numerous additional maintenance discrepancies with the airplane; however, none of these would have contributed to a loss of engine power. According to the inspectors, the airplane's most recent annual inspection was completed on March 19, 2008.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX08LA142