N1510A

Substantial
Serious

Schweizer 300CS/N: 1886

Accident Details

Date
Monday, June 2, 2008
NTSB Number
LAX08CA138
Location
Ogden, UT
Event ID
20080627X00938
Coordinates
41.354721, -112.006385
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
1
Total Aboard
2

Probable Cause and Findings

The pilot under instruction's encounter with a settling with power condition, and the flight instructor's failure to maintain adequate rotor rpm during the subsequent go-around. Also causal was the instructor pilot's delayed remedial action during the approach sequence and his inadequate supervision of the flight.

Aircraft Information

Registration
N1510A
Make
SCHWEIZER
Serial Number
1886
Engine Type
Reciprocating
Year Built
2006
Model / ICAO
300CH269
Aircraft Type
Rotorcraft
No. of Engines
1

Registered Owner (Historical)

Name
HIGH DESERT HELICOPTERS LLC
Address
3477 AIRPORT RD BOX A-9
Status
Deregistered
City
OGDEN
State / Zip Code
UT 84405
Country
United States

Analysis

In a written statement, the instructor pilot reported that he and the private pilot under instruction performed a normal takeoff and departure. After a short flight they arrived at Rocky Point (9 miles north of Ogden-Hinckly Airport), where they were to practice pinnacle approaches and landings. They reconnoitered the area at 300 feet above ground level (agl) in preparation for landing. They performed a power check at 500 feet agl, and concluded that engine power was sufficient to maintain an out of ground effect (OGE) hover. The student began the approach at 350 feet agl. The approach became slightly steep and went past the point of the intended landing. The pilot under instruction reported that the rate of descent was 500 feet per minute (fpm) at 25 knots. At 30 feet agl, the helicopter's descent rate increased, the pilot under instruction aborted the approach, and began a go-around. The instructor realized that rotor revolutions-per-minute (rpm) had degraded below the normal range, so he took the controls from the student. Because the go-around had been initiated, the helicopter was moving forward slowly over a descending hill slope and the instructor was not able to land the helicopter. He attempted to gain power by lowering and raising collective; however, the helicopter's skid contacted the ground and the helicopter rolled over.

FAA-H-8083-21, Rotorcraft Flying Handbook, states that vortex ring state (settling with power) is likely when the rate of descent exceeds 300 fpm, and the horizontal velocity is slower than effective translational lift.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX08CA138