N587X

Destroyed
Fatal

CONVAIR CV-580S/N: 361

Accident Details

Date
Monday, September 1, 2008
NTSB Number
CHI08MA270
Location
Columbus, OH
Event ID
20080909X01418
Coordinates
39.798332, -82.979164
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
3
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
3

Probable Cause and Findings

The improper (reverse) rigging of the elevator trim cables by company maintenance personnel, and their subsequent failure to discover the misrigging during required post-maintenance checks. Contributing to the accident was the captain’s inadequate post-maintenance preflight check and the flight crew’s improper response to the trim problem.

Aircraft Information

Registration
N587X
Make
CONVAIR
Serial Number
361
Year Built
1956
Model / ICAO
CV-580

Registered Owner (Historical)

Name
AIR TAHOMA INC
Address
26117 34TH AVE E
Status
Deregistered
City
SPANAWAY
State / Zip Code
WA 98387-9439
Country
United States

Analysis

HISTORY OF FLIGHT

On September 1, 2008, about 1206 eastern daylight time, a Convair CV-580 airplane, N587X, operated by Air Tahoma Inc., was destroyed when it impacted terrain as it was attempting to return to the Rickenbacker International Airport (LCK), Columbus, Ohio. The flight had just departed from runway 5L (11,937 feet by 150 feet, asphalt) at LCK. The captain, first officer, and a company pilot sitting in the observer seat received fatal injuries. The 14 Code of Federal Regulations Part 91 post maintenance check flight departed LCK at 1203, and was en route to Mansfield Lahm Regional Airport (MFD), Mansfield, Ohio. Visual meteorological conditions prevailed at the time of the accident. An instrument flight rules (IFR) flight plan was filed.

The accident flight was the first flight following a maintenance Phase 1 and Phase 2 check, which included flight control cable rigging as part of the check. The flight was also intended to provide cockpit familiarization for the first officer and the observer, and a training flight for the first officer.

The flight contacted LCK air traffic control (ATC) at 1139 for its IFR clearance. At 1147, the flight was cleared to taxi. At 1200, the flight received its takeoff clearance, and the airplane started its takeoff roll about 1203.

About one minute later at 1204, the flight contacted ATC and stated that it needed to return to LCK. It was cleared to land on runway 5L. ATC asked the flight if it needed equipment and the flight responded, "Negative."

Radar track data indicated that about 1204, the airplane was mid-downwind for runway 5L about 900 feet above ground level (agl) with a 171-knot ground speed. When the airplane was approximately turning to the base leg, it was about 187 feet agl on a southerly heading with a 196-knot ground speed. About 1206, the airplane impacted a cornfield about one mile southwest of the approach end of runway 5L.

PERSONNEL INFORMATION

The captain was an airline transport pilot with multi-engine land and instrument airplane ratings. He held a first-class medical certificate that was issued on July 23, 2008. The captain's total flight time as recorded on his last medical certificate application was 16,087 hours. According to company records, he had flown 170 hours in the Convair (CV) 580 in the last 90 days and 46 hours in the last 46 days. He held airplane type ratings in the following aircraft: Boeing B-727, CV-340, -440, and -580's, Grumman G-100, Lockhead L-382, and IA-1125. He had completed the 6-month proficiency check in the CV-580 on May 17, 2008. On July 16, 2008, the captain was designated by the Federal Aviation Administration (FAA) as a CV-580 Check Airman for employees of Air Tahoma Inc.

The first officer was an airline transport pilot with single-engine and multi-engine land and instrument airplane ratings. He held a first-class medical certificate that was issued on August 6, 2008. The first officer's total flight time as recorded on his last medical certificate application was 19,285 hours. He held airplane type ratings in the following aircraft: Boeing B-727, CV-240, -340, and -440's, McDonnell Douglas DC-4, -7 and -8's, and Lockhead L-1011's.

The observer pilot on the flight was a commercial pilot with single-engine and multi-engine land and instrument airplane ratings. He held a first-class medical certificate that was issued on April 4, 2008. His total flight time as recorded on his resume submitted to Air Tahoma was 498 hours. He also held an Airframe and Powerplant (A&P) certificate and a Flight Engineer certificate.

Air Tahoma hired the first officer and the observer pilot on August 27, 2008, to fill the positions of captain and first officer, respectively. Both were going through the Initial New Hire training program. As of August 30, both had completed 28.5 hours of aircraft systems training which required a total of 63 hours for completion.

The Air Tahoma FAA approved CV-580 Flight Crew Training Manual issued in July 2005 stated the following concerning training progression: "Personnel in training will only be advanced to a higher level after all lower levels have been satisfactorily completed. This applies to all training." The training manual indicated that Basic Indoctrination and Aircraft Systems required completion prior to Flight Training. Air Tahoma's proposed training manual issued September 2007, but not approved by the FAA, stated the following concerning training progression: "Normally, personnel in training will only be advanced to a higher phase after all lower phases have been satisfactorily completed." It further stated, "Progression for subjects listed in paragraph A may be changed if it is in the best interest of the Company."

AIRCRAFT INFORMATION

The airplane was a Convair CV-580, serial number 361, manufactured in 1956 as a 56-seat passenger airplane that was converted to a cargo airplane. The airplane was modified by Supplemental Type Certificate (STC) SA4-1100 with the addition of the two Allison 501-D13D turboprop engines that each produced 3,800 shaft horsepower. The airplane had a maximum gross weight of 58,156 pounds. The last phase inspection was conducted on August 18, 2008. The total airframe time was 71,990.4 hours. The accident flight was the first flight after the phase inspection was completed.

An examination of the Phase 1 and Phase 2 cards used to conduct the phase inspection completed on August 18, 2008, revealed that the inspector's block on numerous checks were not signed off by the Required Inspection Item (RII) inspector. The RII inspector did not sign the Phase 2, card 55-04, item 59a, 59b, 59c, and 59d. Item 59b states, "Connect elevator servo trim tab cables and rig in accordance with Allison Convair M/M, section 8, figure 8.2.108 and 8.2.108A." The item had been signed off by the mechanic, but not by the RII inspector. The Phase 2 card also contained a NOTE, which stated in bold type, "A complete inspection of all elevator controls must be accomplished and signed off by an RII qualified inspector and a logbook entry made to this effect." The RII inspector block was not signed off.

The examination of the airplane's logbook indicated that the aircraft was released for flight on August 8, 2008. The discrepancy side of the logbook page listed, "AT-23's as required." (AT-23 cards are discrepancy cards used during aircraft maintenance.) The corrective action side of the form stated, "Complied with all AT-23's as required." On July 25, 2008, an AT-23 card, control number 10544, indicated that the right hand horizontal elevator was removed and reinstalled in accordance with the maintenance manual 27-30-0 to facilitate other maintenance. The AT-23 card, control number 10544, had both the mechanic's and the RII's signature.

The airplane was not flown on August 8, 2008, and did not fly until the accident flight on September 1, 2008. The airplane's logbook indicated that that there were no discrepancies entered into the logbook from August 8 - September 1, 2008, that specifically identified that the elevator trim system had received maintenance or needed to be checked prior to flight. The airplane received a service check on September 1, 2008, and was released for flight.

METEOROLOGICAL INFORMATION

At 1157, the surface weather observation at LCK was: Winds 080 at 3 knots, visibility 7 miles, clear skies, temperature 28 degrees Celsius (C), dew point 18 degrees C, altimeter 30.18 inches of Mercury.

FLIGHT RECORDERS

The Cockpit Voice Recorder (CVR) and Flight Data Recorder (FDR) were retrieved from the tail section of the wreckage and were sent to the National Transportation Safety Board's (NTSB) Vehicle Recorder Division for inspection.

The FDR was downloaded and approximately 4 hours of data was transcribed. A review of the data showed that the accident flight was not recorded by the FDR. The accident airplane was equipped with a switch in the cockpit to provide power to the FDR. Selection of the FDR switch was a checklist item that required the pilots to select the FDR switch to ON. The CVR tape indicated that the pilots skipped over the checklist item that called for the FDR switch to be selected to the ON position. The CVR recording indicated that there was no discussion between the pilots concerning the FDR switch, whether it should be in the ON or OFF position. The panel that contained the FDR switch was not located in the wreckage.

The CVR recorded 33-minutes, 11-seconds of useable audio information. The recording and prepared transcript began at 1132:47 and covered the preflight, taxi, takeoff, and accident events. The recording and transcript ended at 1205:58. The CVR indicated that during the conversations recorded by the CVR, the pilots did not discuss any special or extra requirements to conduct flight control checks as a result of the maintenance performed on the elevator and rudder.

From 11:33:03 to 12:00:47, the captain, first officer, and the observer were going through the cockpit checklists in preparation for takeoff. As they went through the checklist, the captain pointed out to the first officer and observer where particular gauges, switches, or instruments were located in the cockpit. At 12:00:47, the tower cleared the airplane for takeoff. The CVR indicated that the airplane was taxied onto the runway and the flight crew did power checks of the engines prior to takeoff. At 12:03:18, the first officer transmitted to tower that the airplane was commencing its takeoff roll.

The CVR indicated that the duration of the accident flight from the time of the takeoff roll until the sound of impact was about 2 minutes 40 seconds. During the accident flight, neither the captain nor the first officer called for the landing gear to be raised, the flaps to be retracted, or the power levers to be reduced from full power. From the time the first officer called "rot...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI08MA270