N411EV

Substantial
None

Evektor Aerotechnik AS SportstarS/N: 2005-0411

Accident Details

Date
Tuesday, August 5, 2008
NTSB Number
DFW08LA209
Location
St Charles, MO
Event ID
20080922X01510
Coordinates
38.842498, -90.500000
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The student pilot's failure to maintain control due to his task saturation as a result of his failure to set the pitch trim to the neutral position before takeoff.

Aircraft Information

Registration
N411EV
Make
EVEKTOR AEROTECHNIK AS
Serial Number
2005-0411
Engine Type
Reciprocating
Year Built
2005
Model / ICAO
SportstarEVSS
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
REGISTRATION PENDING
Address
16321 COUNTRY RD
Status
Deregistered
City
CANYON
State / Zip Code
TX 79015-5891
Country
United States

Analysis

On August 5, 2008, at approximately 1500 central daylight time (CDT), a Evektor-Aerotechnik AS Sportstar, N411EV, registered to Stearns-Chatten LLC and operated by St. Charles Flying Service, Inc. as a 14 Code of Federal Regulations Part 91 flight, was substantially damaged following a hard landing at St. Charles Airport (K3SQ), St, Charles, Missouri. Visual meteorological conditions prevailed and flight plan had not been filed. The special light sport airplane was substantially damaged by the impact forces. The student pilot, who was the only occupant, reported no injuries.

In a statement provided by the student pilot, he reported use of the checklist and a normal takeoff. While 75 to 100 feet above the runway the airplane had a “sudden plunge” but the student pilot was able to pull back on the control stick to regain control of the airplane. A similar nose-over event occurred as he turned crosswind, but was once again able to regain control. The student pilot stated that he "sensed that (he) was in big trouble” and he “needed to get the plane back on the ground as quickly as possible”. The airplane continued to exhibit a nose-over tendency throughout the traffic pattern to runway 09. While turning to final, the student pilot realized that the power setting was too high, but he could not simultaneously maintain aircraft control and adjust the power setting, so the airplane's airspeed remained higher than normal. The airplane touched down at “high speed” and “hit the runway very hard”. The pilot lost directional control after touchdown and the airplane departed the left side of the runway, traveled through the grass and nosed over.

An on-scene investigation was performed by inspectors from the Federal Aviation Administration (FAA). No pre-existing anomalies were discovered with the airframe or the engine. However, the pitch trim was found in the full nose-down position. The pitch trim system and flight controls were examined and found to operate normally.

When the FAA inspectors interviewed the student pilot and asked him to describe his cockpit checks prior to take-off he did not mention the elevator trim setting during any of the checks. Then, when asked if he had possibly left the elevator trim at the wrong setting he responded “I supposed it is… I didn’t even think about the trim tab”.

The student pilot reported a total of 40 hours of experience with approximately 25 hours in the same make and model as the accident airplane. His most recent flight was on June 23, 2008, approximately 6 weeks prior to the accident flight.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# DFW08LA209