N301KC

Substantial
None

MOONEY M20JS/N: 24-0414

Accident Details

Date
Monday, September 8, 2008
NTSB Number
NYC08LA311
Location
Hackettstown, NJ
Event ID
20080922X01517
Coordinates
40.818611, -74.853057
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot's failure to adhere to the airplane manufacturer's published preflight inspection procedures, enabling water to remain undetected in the fuel system, which resulted in a complete loss of engine power immediately after takeoff.

Aircraft Information

Registration
Make
MOONEY
Serial Number
24-0414
Engine Type
Reciprocating
Year Built
1978
Model / ICAO
M20JM20P
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
M20J

Registered Owner (Current)

Name
RIDL KENT S
Address
1638 19TH AVE E
City
WEST FARGO
State / Zip Code
ND 58078-4321
Country
United States

Analysis

HISTORY OF FLIGHT

On September 8, 2008, about 1630 eastern daylight time, a Mooney M20J, N301KC, was substantially damaged during an emergency landing immediately after takeoff from runway 23 at Hackettstown Airport (N05), Hackettstown, New Jersey. The private pilot, who was the sole occupant, was uninjured. The positioning flight was operated under the provisions of 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed, and no flight plan had been filed.

According to the pilot, he was an aircraft broker, and he was repositioning the airplane for the owner from its base at Essex County Airport (CDW) Caldwell, New Jersey, to another airport, in conjunction with the possible sale of the airplane. The pilot stated that he did not add any fuel to the airplane at CDW, and that he activated all three fuel drains prior to the flight. He did not observe any water in the fuel samples that he captured from the two wing tanks. The pilot did not capture a sample when he drained the gascolator, since the gascolator drain was activated from the cockpit. Engine start and run-up were normal, and the airplane departed CDW for Sky Manor Airport (N40) Pottstown, New Jersey, where the pilot stopped to pick up an acquaintance. The pilot and his passenger then flew from N40 to N05. Both flights were uneventful.

After they arrived at N05, the passenger left the pilot, in order to depart in a different airplane. The pilot then dispensed 21.6 gallons of fuel from the self-service facility at N05 into the right wing tank, but he did not add any to the left wing tank, since it was still full. At the time of the fueling, the airplane was parked in an area which resulted in an airplane-nose-down attitude. Subsequent to the fueling, the pilot sampled fuel from the right tank drain, and he did not observe any water. He also activated the cockpit control to drain the gascolator, but again he did not capture the gascolator sample.

Engine start and taxi were normal. The pilot planned to depart using runway 23, so he taxied to the runway, turned the airplane to a heading of approximately north for the engine run-up, and stopped the airplane. At this point, the airplane was in a slightly left-wing-down attitude. The pilot stated that for the engine run-up and takeoff, fuel was supplied to the engine from the right wing tank, and that the run-up was normal. He also stated that he began the takeoff attempt about 45 minutes after the fueling was completed. According to the pilot, the takeoff roll and initial climb were normal, but when the airplane reached approximately 25 feet above ground level, the engine "quit dead."

The pilot added that due to the short amount of pavement that remained ahead on runway 23, he initiated a turn to the left in an attempt to use a "crossing runway" for the emergency landing and rollout. However, the airplane did not have sufficient altitude or airspeed to complete the turn, so the pilot leveled the wings, touched down in the grass approximately 20 feet off the left side of runway 23, and applied "heavy braking." The airplane impacted trees and shrubs that bordered the airport, and came to a stop.

After the accident, the pilot sampled the fuel from the gascolator and the two wing tank drains. He stated that he used a "16 ounce Coke bottle," and that he captured approximately "1 to 1 1/2" inches of water from the gascolator. He used a fuel drain cup that measured approximately 2 inches high by 1 1/2 inches in diameter, and obtained two cupfuls of water from the right tank. The pilot did not observe any water in the sample that he obtained from the left tank.

PERSONNEL INFORMATION

According to Federal Aviation Administration (FAA) and pilot-provided information, the pilot held a private pilot certificate with airplane single- and multiengine land ratings. He had approximately 4,000 total hours of flight experience. His most recent FAA third-class medical certificate was issued in March 2007.

According to the owner of the airplane, the pilot was recommended to him by a large aircraft sales company which specialized in Mooney airplanes. Due to the recommendation, and the fact that the pilot told the owner that he had "substantial Mooney time," the owner did not ask the pilot for details of his experience. The owner stated that the pilot had possession of the airplane for about 2 to 3 months prior to the accident, that he (the owner) did not fly the airplane during this period, and that he (the owner) was not aware of the pilot's flight activity in the airplane during that period.

The NTSB was unable to determine the pilot's experience in the accident airplane make and model. Despite verbal assurances from the pilot that he would comply with multiple NTSB requests for additional information regarding his experience, qualifications, and the events of the day, the pilot did not provide the requested information.

AIRCRAFT INFORMATION

The airplane was a low-wing monoplane of all-metal construction. It was equipped with a Lycoming IO-360 four-cylinder engine, a constant-speed propeller, and retractable tricycle-style landing gear. According to FAA information, the airplane was manufactured in 1978, and it was purchased by the current owner in 1998. The owner reported that the airplane had approximately 2,760 total hours in service, and that the most recent annual inspection was accomplished in December 2007.

METEOROLOGICAL INFORMATION

The 1554 surface weather observation at Aeroflex-Andover Airport (12N), Andover, New Jersey, located 13 miles northeast of N05, reported variable winds at 6 knots with gusts to 16 knots, temperature 27 degrees C, dew point 11 degrees C, and an altimeter setting of 30.12 inches of mercury. The 1654 observation reported similar conditions.

AIRPORT INFORMATION

According to FAA and commercially-available information, N05 was equipped with only a single runway. Runway 5/23 was asphalt, measured 2,200 feet by 50 feet, and was dry at the time of the accident. Examination of aerial photographs of the airport revealed that the grassy area that was bounded by the southern portion of the treeline along the southeast side of the airport had two rectangular extensions which were similar in appearance to defunct runways. One extension was oriented perpendicular to runway 23, along a heading of approximately 140 degrees. The other extension was oriented approximately 50 degrees to the southeast of runway 23, along a heading of approximately 180 degrees. Each of these extensions was approximately 800 feet long, and 200 feet wide.

WRECKAGE AND IMPACT INFORMATION

According to FAA information, the airplane was stopped by the treeline that was perpendicular to the runway centerline, and situated approximately 100 feet beyond the end of the paved runway surface. The airplane was offset approximately 100 feet southeast of the runway centerline. It remained upright, and all three landing gear were intact. The outboard 2 feet of the left wing were fracture-separated from the wing, and remained attached to the wing by the inboard hinge of the left aileron. The wing skin and underlying structure just inboard of the separation line was crushed aft and up. The right wing bore three crush damage sites that began at the leading edge and extended aft. The skin at the inboard site was crushed approximately 8 inches aft of the leading edge. The skin and underlying structure at the mid and outboard sites was crushed and torn for nearly the full chord of the wing. The right and upper sides of the aft fuselage sustained buckling damage, and the propeller spinner sustained crush damage in the aft direction. There was no fire.

ADDITIONAL INFORMATION

Airplane Fuel System Configuration

According to the airplane manufacturer, each fuel tank consisted of an integral sealed bay in the inboard section of each wing. The total usable fuel capacity was 64 gallons, and each tank had an unusable fuel quantity of 1.25 gallons. The inboard and outboard walls of each tank were the wing ribs at wing station (WS) 24.5 and WS 74.0, respectively. The forward tank wall was formed by webs and baffles aft of the wing leading edge, and the aft tank wall was the main wing spar. Internal tank ribs at WS 43.5 and WS 59.25, which extended for the full chord of the tank, also functioned as anti-slosh baffles. A discontinuous stringer, located midway between the forward and aft tank walls on the tank floor, extended spanwise from the inboard tank wall to the outboard tank wall. The inboard stringer segment ran from the inboard tank wall, through a cutout in the WS 43.5 rib, to the WS 59.25 rib, and the outboard segment ran from the WS 59.25 rib to the outboard tank wall.

Each tank's internal structure was designed to enable the fuel to reach the fuel pickup point, and to allow any water in the tank to reach the tank sump drain point. Each of the WS 43.5 and WS 59.25 ribs had four large, circular lightening holes in their webs. Each WS 43.5 rib had eight 1/4-inch diameter holes distributed chordwise just above its juncture with the tank floor; four were forward of the stringer, and four were aft. Each WS 59.25 rib had one 1/4 by 1/2-inch oval hole, and five 1/4-inch circular holes, distributed chordwise just above its juncture with the tank floor; three circular holes were forward of the stringer, and the other three holes were aft of the stringer. The standing leg of each stringer segment was approximately 3/4 inch high. Each inboard stringer segment had two holes located between the inboard tank wall and the WS 43.5 rib, and two more located between the WS 43.5 rib and the WS 59.25 rib. The outboard stringer segments did not have any similar drain holes.

Each fuel tank was equipped with a flush-fitting fuel cap, and each cap utilized an O-ring to preclude water intrusion through the cap-tank juncture. A fuel selector valve in the cockpit enabled a pilot to select one of three possible se...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# NYC08LA311