N272RS

Substantial
None

Brennan RV-8S/N: 81896

Accident Details

Date
Wednesday, October 1, 2008
NTSB Number
SEA08LA216
Location
Idaho Falls, ID
Event ID
20081006X60439
Coordinates
43.063610, -112.070556
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The on-ground fire during taxi due to a loose fuel line "B" nut.

Aircraft Information

Registration
N272RS
Make
BRENNAN
Serial Number
81896
Engine Type
Reciprocating
Model / ICAO
RV-8RV8
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Analysis

On September 30, 2008, about 1825 mountain daylight time, an amateur built Brennan RV-8 experimental airplane, N272RS, was substantially damaged by an on-ground fire while taxiing for departure at the Idaho Falls Regional Airport (IDA), Idaho Falls, Idaho. The airplane was registered to and operated by the pilot under the provisions of Title 14 Code of Federal Regulations (CFR) Part 91 with no flight plan filed. Visual meteorological conditions prevailed. The commercial pilot and his passenger were not injured. The cross-country personal flight was originating at the time of the accident with a planned destination of Heber, Utah.

The pilot reported that while taxiing to the runway for departure, he noticed flames entering the cockpit below his feet. He immediately stopped the airplane and shut the engine down as he and his passenger exited the airplane. The airport's Aircraft Rescue Fire Fighting (ARFF) team responded and extinguished the fire, which was originating from the engine compartment. A few minutes later, the fire reportedly ignited a second time and was immediately extinguished by ARFF personnel.

Examination of the airplane by a Federal Aviation Administration (FAA) inspector revealed that the firewall was severely fire damaged and buckled. The engine compartment and forward portion of the fuselage were thermally damaged.

Examination of the airplane by a local mechanic revealed that a "B" nut attaching the firewall end of the fuel line from the firewall to the engine driven fuel pump was found "finger tight." When the airplane was placed in a tail high attitude, fuel was observed leaking from this fitting. The mechanic stated that after the ARFF team extinguished the fire, he disconnected the battery. Prior to disconnecting the battery, he noted that the electric fuel boost pump was on. The reason for the loose "B" nut was undetermined.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA08LA216