N6TR

Substantial
Serious

NICKEL RV-6S/N: 20492

Accident Details

Date
Tuesday, November 25, 2008
NTSB Number
WPR09LA047
Location
Fresno, CA
Event ID
20081126X31943
Coordinates
36.840000, -119.869163
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The loss of engine power during initial climb for undetermined reasons.

Aircraft Information

Registration
N6TR
Make
NICKEL
Serial Number
20492
Engine Type
Reciprocating
Year Built
0000
Model / ICAO
RV-6RV6
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SALE REPORTED
Address
NONE
Status
Deregistered
City
XXXX
State / Zip Code
OK 73125
Country
United States

Analysis

On November 25, 2008, about 1530 Pacific standard time, a Nickel RV-6 amateur-built experimental airplane, N6TR, sustained substantial damage during a forced landing following a loss of engine power after takeoff from Sierra Sky Park Airport, Fresno, California. The private pilot, the sole occupant, who was the owner and builder of the airplane, was seriously injured. Visual meteorological conditions prevailed, and no flight plan was filed for the local personal flight conducted under 14 Code of Federal Regulations Part 91. The flight was originating when the accident occurred.

The pilot reported that prior to takeoff; he performed a high-speed taxi test on the runway with no anomalies noted. The pilot taxied back to the run-up area, performed his preflight checklist uneventfully, and proceeded to takeoff. During the takeoff initial climb, the engine misfired and developed "marginal power." As he executed a left turn towards the airport, the engine lost power. The pilot further stated "to take advantage of relatively good landing opportunities below," he continued the left turn and initiated a forced landing to an open area on a golf course. During the landing roll, the airplane struck a berm and became airborne again. Subsequently, the airplane landed hard and came to rest upright.

Examination of the airplane by a Federal Aviation Administration inspector revealed that the airplane came to rest within a golf course about 1 mile northwest of the runway. The engine was partially separated from the airframe, and the firewall was bent and buckled.

Examination of the converted Ford engine by the pilot revealed the fuel system was intact and undamaged. The pilot also reported finding "no obvious" anomalies with the ignition system. The reason for the loss of engine power was not determined.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR09LA047